QFR No - 8000808151
Defect Details
NC No. | 8000808151 |
NC Date | 17/10/2022 |
NC Submission Date | |
Part No. | S2BG03908B |
Part Name | BKT POWDER COATED |
Supplier Name & Code | 101032-ASM CASTINGS PRIVATE LIMITED ( |
ETL Plant | 1116-ETL K-120 Suspension |
Defect Details | THREADING NOT OK-THREADING NOT OK |
1. Problem Description
Defect Description | KHI Bracket observed with step at ID side concern. This causing assembly fitment (Rubber bush fitment) not OK. |
Detection Stage | Inprocess |
Problem Severity | Fitment |
NG Quantity | 553 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | quality@asmcastings.in |
Plant Head/CEO Email ID | skaul@asmcastings.in |
MD Email ID | rajiv@asmcastings.in |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
2000
|
1200
|
0
|
2800
|
0
|
6000
|
Check Qty |
2000
|
1200
|
0
|
2800
|
0
|
6000
|
NG Qty |
553
|
128
|
0
|
221
|
0
|
902
|
Scrap | 902 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
100% Segregation at customer as well as ASM End. |
3. Process Flow
Process Flow Description |
---|
R.M. Receiving - Die Casting - Fattling - Bush Fitting Dia Reamer - Drilling & Tapping - Visual Inspection - PDI -Packing - Dispatch - Powder Coating at Tulza Ent. - Dispatch to ETL. |
4. Process Details
Process / Operation | Powder Coating |
Outsource | Yes |
Machine / Cell | Die Casting |
Machine / Cell No. | PDC-01 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Material | Hard Particle in Al Ingot. | Chemical Composition | O |
Method | Reamer not adequate | Remer Size Checked | O |
Man | Un Skilled Operator | Skill Matrix | O |
Tool | Pin Bulged in Die | Physical Verification | X |
Machine | Play in Machine Platon | Physical Verification | O |
6. Inspection Method Analysis (Current)
Inspection Method | Instrument |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 05 Nos. |
7. Root Cause Analysis (Occurance)
Why 1 | Step Observed in ID |
Why 2 | Pin Bulged during Mass Production |
Why 3 | Not Checked in Process Inspection |
Why 4 | Check Point not added in Inspection td. |
Why 5 | |
Root Cause (Occurance) | Check point not added in Inspection Std. for Step in I.D. |
Root Cause Analysis (Outflow)
Why 1 | Step in I.D. |
Why 2 | Could Not detected during Final Inspection |
Why 3 | Inspector Not aware about Issue. |
Why 4 | Check Point not added in Work Instruction. |
Why 5 | |
Root Cause (Outflow) | Check For Step in I.D. , not added in Work Instruction of Final Inspection. |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Check Point added for Step In I.D. in Inspection Std. of PDC. | Lalit Sharma | 10/11/2022 | Completed | |
Outflow | Check Point added in Work Instruction of Final Inspection | Lalit Sharma | 10/11/2022 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | Earlier Limit Sample was not there for Compare |
Inspection Method | Other |
Other Inspection Method | Limit Sample. |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
No Check Point at PDC stage for Step in I.D. 288_Occurance_Before.jpg |
Occurance (After) |
Check Point added for step in ID at PDC Stage 288_Occurance_After.jpg |
Outflow (Before) |
No Check Point for Step in I.D. in Work Instruction & No Limit Sample 288_Outflow_Before.jpg |
Outflow (After) |
Check point added in Work Instruction at Final Stage & Limit Sample Provided. 288_Outflow_After.jpg |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | PDC Machine |
12. Document Review
Documents | ControlPlan, PFMEA, WISOP, InspCheckSheet |
Specify Other Document | Limit Sample |
13. Effectiveness Of Action
Reviewed Quantity | 1000 |
Reason for submission | No any reoccurance. |