QFR No - 8000808154
Defect Details
NC No. 8000808154
NC Date 17/10/2022
NC Submission Date
Part No. 550FA17433
Part Name FORK PIPE MACHINED
Supplier Name & Code 100503-DIVYA INDUSTRIES
ETL Plant 1116-ETL K-120 Suspension
Defect Details NOT AS PER SPECIFICATION-THREADING,CLUCKING,LENGTH NOTOK
 
1. Problem Description
Defect Description Dimensional NG concern:- During assembly operation fitment parameters, like threading, caulking ID, total length observed not ok.
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 114
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID quality@mahavirind.co.in
Plant Head/CEO Email ID production@mahavirind.co.in
MD Email ID rajesh@mahavirind.co.in
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
2600
0
0
0
0
2600
Check Qty
2600
0
0
0
0
2600
NG Qty
114
0
0
0
0
114
 
Scrap 10
Rework 104
Under Deviation 0
Containment Action
All material Segregation at Customer End
 
3. Process Flow
Process Flow Description
1)RM pipe Cutting Inward- 2)Store- 3)CNC 1st Caulking Side Machining -4)CNC 2nd side Machining -5) F1.5mm Drilling --6) Final Inspection -7) Packing -Dispatch
 
4. Process Details
Process / Operation 3)CNC 1st Caulking Side Machining
Outsource No
Machine / Cell Fork Pipe CNC machine Shop.
Machine / Cell No. CNC-5
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MaterialFork Pipe face Unclean / Depth Under Size By0.2 -0.5Length Under Size by 0.2-0.5 of Fork Pipe Raw MaterialX
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size ..........
7. Root Cause Analysis (Occurance)
Why 1 Caulking Depth Under size
Why 2 Caulking Side Face Unclean
Why 3 CNC-1st Side - Caulking Side Facing Not Proper as Require Length
Why 4 Raw Material Length Short
Why 5
Root Cause (Occurance) Raw Material Length Short
 
Root Cause Analysis (Outflow)
Why 1 Caulking Depth Under size
Why 2 Face Unclean Defect Not Detect During Final Inspection
Why 3 Inspector Not Aware Of Face Unclean
Why 4 New Inspector
Why 5
Root Cause (Outflow) Inspector Not Aware Of Face Unclean
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
Outflow1)Raw material Length Short. 2)New Final Inspector.Mr Gadekar And Mr. Suresh Kapgate20/10/202220/10/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 1) Defected Samples display at Final Inspection And Machine .2) OJT to Machine Operator & New Inspector.
Inspection Method Sp. Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size ...
10. Evidance of Countermeasure
Occurance (Before) Caulking Side face Unclean / Caulking side Depth Under Size
289_Occurance_Before.jpeg
Occurance (After) One Point Lesson Display / OJT to operators
289_Occurance_After.xlsx
Outflow (Before) Raw Material Length Short form Source Area
289_Outflow_Before.jpeg
Outflow (After) Ram material Inspection start
289_Outflow_After.xlsx
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant All Types Fork Pipe
 
12. Document Review
Documents ControlPlan, PFMEA, InspCheckSheet
Specify Other Document Raw material Inward
 
13. Effectiveness Of Action
Reviewed Quantity
Reason for submission