QFR No - 8000808350
Defect Details
NC No. 8000808350
NC Date 18/10/2022
NC Submission Date
Part No. 013AQ00123
Part Name BASE VALVE CASE GROOVED
Supplier Name & Code 100177-SPECIALITY SINTERED PRODUCTS P
ETL Plant 1116-ETL K-120 Suspension
Defect Details NOT AS PER SPECIFICATION-OPRATION MISSING
 
1. Problem Description
Defect Description Groove operation missing concern repetitively observed.
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 8
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID ganeshpadwalkar@specialitysintered.com
Plant Head/CEO Email ID sandeep.gaikwad@ssplpune.com
MD Email ID lalit.chaudhari@ssplpune.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
20000
30000
0
15000
12000
77000
Check Qty
19994
30000
0
15000
12000
76994
NG Qty
6
0
0
0
0
6
 
Scrap 6
Rework 0
Under Deviation 0
Containment Action
SSPL representative visited to ETL for ICA at ETL End and Warehouse
 
3. Process Flow
Process Flow Description
Raw material inspection & Mixing - Forming - Sintering - Debarring - Steam - machining - Final Inspection - Oiling - Packagining - Dispatch
 
4. Process Details
Process / Operation Machining
Outsource Yes
Machine / Cell Traun No 10
Machine / Cell No. Traub section
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ManUnskill OperatorLevel 4 Operator At Machine .X
MethodInput & Material Handling Not OkVerified No seprate Provision Provided To Unlodade Output Material.O
ToolWrong Tool UsedTool Verified Found OkX
MaterialWrong Raw MaterialMaterial Checked As Per TC Found OkX
MachineMachine Not Working ProperlyVerified Found OkX
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size As Per Sam
7. Root Cause Analysis (Occurance)
Why 1 Without Machining Part Found At Customer End ..
Why 2 During Machining process Machine Input Material Mixed With Output Material. .
Why 3 No seprate Provision Provided To Unlodade Output Material.
Why 4 No Poke Yoka .
Why 5
Root Cause (Occurance) No Poke Yoka .
 
Root Cause Analysis (Outflow)
Why 1 Without Machining Part Found At Customer End .
Why 2 Deffective part Pass from Final Inspection .
Why 3 Rejected parts Mixed With Ok Parts .
Why 4 Lock And Key Rejection Bin Not Available At Final Inspection Table .
Why 5
Root Cause (Outflow) Lock And Key Rejection Bin Not Available At Final Inspection Table .
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OutflowLock And Key For Rejection Material Provision Given To Inspection Table .MR Sunil20/10/202221/10/2022Completed
OccuranceSeprate Provision Provided To Unloaded Output material .Mr Mahesh Narkhede25/10/202227/10/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Lock And Key For Rejection Material Provision Given To Inspection Table .
Inspection Method Other
Other Inspection Method Visual Inspection
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) No Separate Provision Provided To Unloaded Output material .
291_Occurance_Before.xlsx
Occurance (After) Separate Provision Provided To Unloaded Output material .
291_Occurance_After.xlsx
Outflow (Before) Lock And Key Provision Not Available For Rejected Material At Inspection Table
291_Outflow_Before.xlsx
Outflow (After) Lock And Key Provision Given For Rejected Material At Inspection Table .
291_Outflow_After.xlsx
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant -
 
12. Document Review
Documents InspCheckSheet
Specify Other Document Quality Alert .
 
13. Effectiveness Of Action
Reviewed Quantity 1200
Reason for submission Completed.