QFR No - 8000808535
Defect Details
NC No. 8000808535
NC Date 19/10/2022
NC Submission Date
Part No. 550LG06202
Part Name SEAT PIPE -K23A/PRFH-006
Supplier Name & Code 100929-HARSHAD ENGINEERING COMPANY
ETL Plant 1116-ETL K-120 Suspension
Defect Details DIMN.O/SIZE.-GROOVE WIDTH OVERSIZE
 
1. Problem Description
Defect Description In PRFH Seat pipe - Groove width observed oversize. (No-go gauge qualifies.)
Detection Stage Receipt
Problem Severity Fitment
NG Quantity 1021
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID qaharshad@miteshauto.com
Plant Head/CEO Email ID sjkadam@miteshauto.com
MD Email ID auto.mitesh@gmail.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
6400
5800
0
8800
9600
30600
Check Qty
6400
5800
0
8800
9600
30600
NG Qty
1011
59
0
117
21
1208
 
Scrap 0
Rework 0
Under Deviation 1208
Containment Action
100 % sorting done for ETL End, HEC WIP & FG material
 
3. Process Flow
Process Flow Description
Cutting-Draw-Forging(Head Formation)-Rough Grinding-CNC (Head, Boring & Tapping)-Punching-Finish Grinding-Final Inspection-Packing-Dispatch
 
4. Process Details
Process / Operation CNC Head Turning
Outsource No
Machine / Cell CNC
Machine / Cell No. CNC 1
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MachineIn CNC Prograam Groove width set to higher sideIn CNC Prograam Groove width observed higher side at the time of insert changeO
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size IS2500
7. Root Cause Analysis (Occurance)
Why 1 Groove width found oversize
Why 2 At the time of insert change, 80 to 90 nos found light NOGO enters due to entry chamfer.
Why 3 In CNC programm groove width set to higher side.
Why 4 To avoid Gr. Width undersize fitment issue.
Why 5 To avoid Gr. Width undersize fitment issue. (entry chamfer minor excess observed in said lot)
Root Cause (Occurance) To avoid Gr. Width undersize fitment issue. (entry chamfer minor excess observed in said lot)
 
Root Cause Analysis (Outflow)
Why 1 Groove width found oversize
Why 2 Part skip in FI
Why 3 100% check not done
Why 4 Sampling done/Inspection method not adequete
Why 5
Root Cause (Outflow) Sampling done/Inspection method not adequete
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceIn CNC programe correction done and width size maintained at mean side and radius at entry point corrected to prevent the over size concern.D.D. Jopale19/10/2022Completed
OutflowGroove width 100% check just before packing to avoid NG part mix-up in lot.Vaibhav Shirsath18/10/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Groove width 100% check
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) In CNC Program Groove width maintain at higher side
286_Occurance_Before.jpg
Occurance (After) In CNC Program Groove width maintain at Mean
286_Occurance_After.jpg
Outflow (Before) Groove width checked on Sampling basis
286_Outflow_Before.jpg
Outflow (After) 100% insp. to be done for Groove width
286_Outflow_After.jpg
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant CNC Machines
 
12. Document Review
Documents
Specify Other Document NA
 
13. Effectiveness Of Action
Reviewed Quantity 1000
Reason for submission Effectiveness observed.