QFR No - 8000811541
Defect Details
NC No. | 8000811541 |
NC Date | 21/11/2022 |
NC Submission Date | |
Part No. | B2BK04703O |
Part Name | CALIPER BODY RAW-YAMAHA CBS |
Supplier Name & Code | 100986-MAP ALLOYS |
ETL Plant | 1159-ETL E-71 Disc Brakes |
Defect Details | DENTS & DAMAGES-CASTING DEFECTS DENT & DAMAGE,BLOW HOLE |
1. Problem Description
Defect Description | Damage |
Detection Stage | Receipt |
Problem Severity | Aesthetic |
NG Quantity | 51 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | vinayak@mapalloys.com |
Plant Head/CEO Email ID | milind@mapalloys.com |
MD Email ID | mapalloys3@gmail.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
3185
|
0
|
0
|
0
|
0
|
3185
|
Check Qty |
3185
|
0
|
0
|
0
|
0
|
3185
|
NG Qty |
51
|
0
|
0
|
0
|
0
|
51
|
Scrap | 51 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
100% Segregation done and awareness training provided |
3. Process Flow
Process Flow Description |
---|
RM inward-Incoming Inspection-Storage of RM- Melting -Metal treatment-DIE PREPARATION & DIE LOADING- .CASTING -RUNNER/RISER CUTTING - 90.FETTLING/Grinding-HEAT TREATMENT- Heat No.Punching & SHOT BLASTING -FINAL INSPECTION-PACKING -STORE & DISPATCH |
4. Process Details
Process / Operation | 90-FETTLING/Grinding |
Outsource | No |
Machine / Cell | 05/02 |
Machine / Cell No. | 05/02 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Man | Casting handling | Casting handling evaluate | O |
Tool | High point on die | High point on die evaluate | X |
Machine | Machine running condition | Machine running condition evaluate | O |
Method | Casting Hanging on trolley | Casting hanging on trolley evaluate | O |
Material | Chemical composition | Chemical composition verified | O |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | Visual |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
7. Root Cause Analysis (Occurance)
Why 1 | Hard flash at parting line |
Why 2 | Gap between both halves of die |
Why 3 | High point on parting surface of die |
Why 4 | Die blue matching frequency inadequate |
Why 5 | |
Root Cause (Occurance) | Die blue matching frequency inadequate |
Root Cause Analysis (Outflow)
Why 1 | No awareness of concern person. |
Why 2 | Limit sample not displayed and no awareness training. |
Why 3 | |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | Limit sample not displayed and no awareness training. |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Die blue matching frequency changed from 6 months to 4 months for high point removal from die surface | Mr.Anil Dhande | 15/03/2023 | 30/03/2023 | Completed |
Outflow | Material handling awareness training and limit sample displayed. | R.Pandey | 15/03/2023 | 30/03/2023 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | 100% visual inspection with dot mark for 3 lots |
Inspection Method | Other |
Other Inspection Method | Visually |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
Blue matching frequency inadequate 306_Occurance_Before.xlsx |
Occurance (After) |
Die blue matching frequency changed from 6 months to 4 months for high point removal from die surface 306_Occurance_After.xlsx |
Outflow (Before) |
No limit sample displayed and awareness training about material handling 306_Outflow_Before.xlsx |
Outflow (After) |
Limit sample displayed and awareness training provided 306_Outflow_After.xlsx |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | GDC machine/Yamaha/2 |
12. Document Review
Documents | ControlPlan, PFMEA, WISOP |
Specify Other Document | no |
13. Effectiveness Of Action
Reviewed Quantity | 432 |
Reason for submission | ok ensure |