QFR No - 8000814130
Defect Details
NC No. 8000814130
NC Date 14/12/2022
NC Submission Date
Part No. 550PC09107
Part Name UNDER BKT M/C (CT100)
Supplier Name & Code 101222-SANGKAJ ENGINEERING PVT LTD- U
ETL Plant 1117-ETL K-228/9 Suspension
Defect Details NOT AS PER SPECIFICATION-STEERING SHAFT SITTING ID UNDERSIZE
 
1. Problem Description
Defect Description Under bracket, steering shaft inserting id found undersize
Detection Stage Receipt
Problem Severity Fitment
NG Quantity 643
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID samadhan@sangkaj.com
Plant Head/CEO Email ID steel@sangkaj.com
MD Email ID anirudh.2007@hotmail.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
800
0
0
200
0
1000
Check Qty
800
0
0
200
0
1000
NG Qty
643
0
0
0
0
643
 
Scrap 0
Rework 643
Under Deviation 0
Containment Action
100% inspection of Pipe line material.
 
3. Process Flow
Process Flow Description
Forging inward --- Pre-drilling ---- VMC 1St setup ---- VMC 2nd setup ---- VMC 3rd Setup ---- VMC 4th setup ----Final Inspection
 
4. Process Details
Process / Operation VMC 1st Setup
Outsource No
Machine / Cell VMC machine
Machine / Cell No. Cell no. 4
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ToolTool Worn OutTool life monitoring not doneO
 
6. Inspection Method Analysis (Current)
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 5
7. Root Cause Analysis (Occurance)
Why 1 Centre Bore ID Undersize
Why 2 Premature Failure Of Insert (Tool)
Why 3 Insert (Tool) Get Wear Out
Why 4 Insert (Tool) life not Monitoring
Why 5 Insert (Tool) life Not Define.
Root Cause (Occurance) Insert (Tool) life Not Define.
 
Root Cause Analysis (Outflow)
Why 1 Centre Bore ID Undersize
Why 2 Not Capture in Final Inspection
Why 3 0.010 mm Dial Bore Gauge used for Final Inspection
Why 4 No Air gauge Used For Final Inspection
Why 5 No Air gauge Used For Final Inspection
Root Cause (Outflow) No Air gauge Used For Final Inspection
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceInsert (Tool) life Not Define.Mr.Dhage28/12/202229/12/2022Completed
OutflowNo Air gauge Used For Final InspectionMr.Pramod Waikos15/01/202318/01/2023Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Air Plug Gauge is used for ID inspection.
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Photo Not Available
321_Occurance_Before.png
Occurance (After) Tool life format
321_Occurance_After.jpeg
Outflow (Before) Bore Gauge is used to inspect the part.
321_Outflow_Before.png
Outflow (After) Air gauge is used to inspect the part.
321_Outflow_After.png
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant CT100, Caliber
 
12. Document Review
Documents ControlPlan, WISOP
Specify Other Document Work Instruction
 
13. Effectiveness Of Action
Reviewed Quantity 300
Reason for submission Verified and found ok next lot