QFR No - 8000814841
Defect Details
NC No. 8000814841
NC Date 20/12/2022
NC Submission Date
Part No. F2FA21433M
Part Name FORK PIPE MACHINED (K17A FF)
Supplier Name & Code 101024-TUBE INVESTMENTS OF INDIA LTD
ETL Plant 1126-ETL Pantnagar
Defect Details DEPTH U/SIZE.-CAULKING DEPTH UNDER SIZE
 
1. Problem Description
Defect Description Caulking depth under size in fork pipe K17
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 235
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID AmitVD@tii.murugappa.com
Plant Head/CEO Email ID guptaajay@tii.murugappa.com
MD Email ID mukeshahuja@tii.murugappa.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
2500
2000
0
0
0
4500
Check Qty
2500
2000
0
0
0
4500
NG Qty
235
5
0
0
0
240
 
Scrap 240
Rework 0
Under Deviation 0
Containment Action
100% segregation done at customer end & 100% segregation done at warehouse
 
3. Process Flow
Process Flow Description
1. Parting 2. CNC Machining First 3. CNC Machining 2nd 4. Drilling
 
4. Process Details
Process / Operation Machining & Drilling
Outsource No
Machine / Cell MACHINE SHOP
Machine / Cell No. CNC MACHINE -01
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodInspection Instruments & Lux LevelInspection with DPG, Lux level- 620O
ManOperatorUntrained operator given Wrong offset in ProgrammeX
MaterialTube Id & Machining MarginAs per Specs.O
ToolTemperature & HumidityNo IssueO
MachineCNC Programme executionProgramme not LockedX
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection No
Checking Freq. 100%
Sampling No
Sample Size 5
7. Root Cause Analysis (Occurance)
Why 1 Fork Pipe Caulking Depth Undersize
Why 2 Depth Less maintained during CNC Machining
Why 3 Due to wrong offset given in the Programme by operator
Why 4 Programme was not Locked
Why 5
Root Cause (Occurance) Operator was Untrained and CNC programme was not Locked, Due to Which wrong offset given in Programme by the Operator.
 
Root Cause Analysis (Outflow)
Why 1 Fork Pipe Caulking Depth Undersize Part received at Customer end
Why 2 Caulking Depth Inspection done on sampling basis.
Why 3 100% Inspection not defined in the WI
Why 4 Because This type of defect not reported in past
Why 5
Root Cause (Outflow) This Parameter was checking on Sampling basis, because This type of defect not reported in past.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
Occurance1. CNC Programme Locked 2. Only Production Supervisor will give the offset. 3. After any correction Quality Line Inspector will recheck the parts and provide approval.TANVEER16/12/202215/12/2022Completed
Outflow1. After every 50Parts, operator will check this parameter with Attribute Gauge. 2. 100% Inspection Started at PDI Stage.TANVEER16/12/202215/12/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 100% Inspection started at PDI Stage
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) CNC Programme Not Locked
323_Occurance_Before.jpeg
Occurance (After) CNC Programme Locked
323_Occurance_After.jpeg
Outflow (Before) After every 50 Parts, operator will check this parameter with Attribute Gauge.ONLY BASIC TRAINING GIVEN
323_Outflow_Before.jpg
Outflow (After) 100% Inspection Started at PDI Stage.
323_Outflow_After.jpg
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant All Models
 
12. Document Review
Documents ControlPlan, PFMEA, WISOP, InspCheckSheet
Specify Other Document QUALITY ALERT
 
13. Effectiveness Of Action
Reviewed Quantity 1
Reason for submission ok