QFR No - 8000817072
Defect Details
NC No. | 8000817072 |
NC Date | 13/01/2023 |
NC Submission Date | |
Part No. | 520LG03002 |
Part Name | SEAT PIPE (K3) |
Supplier Name & Code | 101263-SINGLA PRECISION SCREWS |
ETL Plant | 1117-ETL K-228/9 Suspension |
Defect Details | NOT AS PER SPECIFICATION-BURR BACK SIDE OF DF HOLE (INNER SIDE) |
1. Problem Description
Defect Description | Burr found inside the seat pipe ID (Back side of the DF Hole), causing fitment issue during assembly |
Detection Stage | Receipt |
Problem Severity | Fitment |
NG Quantity | 75 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | quality@singlaprecision.com |
Plant Head/CEO Email ID | quality@singlaprecision.com |
MD Email ID | aditya@singlaprecision.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
1200
|
600
|
0
|
0
|
0
|
1800
|
Check Qty |
1200
|
600
|
0
|
0
|
0
|
1800
|
NG Qty |
75
|
2
|
0
|
0
|
0
|
77
|
Scrap | 75 |
Rework | 2 |
Under Deviation | 0 |
Containment Action |
---|
100 % SEGRATION DONE ON MATERIAL LYING AT VARIOUS STAGES AND MARKING TOBE DONE. |
3. Process Flow
Process Flow Description |
---|
1.R.M INSPECTION 2.HEAD FORGING 3.PUNCHING-1 4.ROUGH GRINDING 5.CNC-1 6.CNC-2 7.COUNTER 8.PUNCHING-II 9. I.D CHIPS REMOVE 10.REAMING (IF NECESSARY) 11.TAPPING 12. FINAL GRINDING 13.CLEANING 14.FINAL INSPECTION 15.PACKING |
4. Process Details
Process / Operation | I.D BURR REMOVING |
Outsource | No |
Machine / Cell | DRILL |
Machine / Cell No. | DRILL05 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Man | UNSKILLED OPERATOR | VALIDATED AND FOUND OK | X |
Tool | DRILL MAY WEAR | VALIDATED AND FOUND OK | X |
Material | RM GRADE NOT OK | VALIDATED AND FOUND OK | X |
Machine | NUT BOLTS MAY LOOSE | VALIDATED AND FOUND OK | X |
Method | BURR MAY FOLD IN I.D | Burr formed during punching operation and stuck in I.D and not visible. It comes out during filing | O |
6. Inspection Method Analysis (Current)
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 5 PCS/HOUR |
7. Root Cause Analysis (Occurance)
Why 1 | Heavy burr found back side of the DF hole. |
Why 2 | Burr formed during punching operation |
Why 3 | It stuck in I.D and not visible |
Why 4 | It comes out during filing and pin operation and rise in I.D |
Why 5 | |
Root Cause (Occurance) | Burr formed during punching operation and stuck in I.D and not visible. It comes out during filing and pin operation and rise in I.D. |
Root Cause Analysis (Outflow)
Why 1 | Inspection plan was not effective. |
Why 2 | NG part skipped from detection |
Why 3 | So NG part dispatched to customer |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | Inspection plan was not effective. NG part skipped from detection .So NG part dispatched to customer |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Outflow | Inspection frequency changed to 100% at final inspection | Ganesh Maurya | 19/01/2023 | 19/01/2023 | Completed |
Occurance | 1- WORK INSTRUCTIONS GIVEN TO OPERATOR AND INSPECTOR REGARDING THE DEFECT OF BURR IN I.D 2. WE STARTED 100% DIA 15.10 mm PIN APPLIED IN I.D TO REMOVE THE BURR. | Ganesh Maurya | 19/01/2023 | 19/01/2023 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | WE STARTED 100% DIA 18.10 mm PIN APPLIED IN I.D TO REMOVE THE BURR. |
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
NO PIN APPLICATION 329_Occurance_Before.jpeg |
Occurance (After) |
PIN APPLIED 329_Occurance_After.jpeg |
Outflow (Before) |
INSPECTION WAS ACC TO SAMPLING 329_Outflow_Before.jpeg |
Outflow (After) |
SAMPLING PLAN CHANGED TO 100% 329_Outflow_After.jpeg |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | All seat pipes |
12. Document Review
Documents | ControlPlan |
Specify Other Document | NO |
13. Effectiveness Of Action
Reviewed Quantity | 100 |
Reason for submission | Ensure 100% inspection with insert pin as per commitment |