QFR No - 8000818063
Defect Details
NC No. | 8000818063 |
NC Date | 23/01/2023 |
NC Submission Date | |
Part No. | F20508007B |
Part Name | UND BKT SUB-ASSEMBLY (K17B/D) |
Supplier Name & Code | 100061-BAJAJSONS LIMITED |
ETL Plant | 1117-ETL K-228/9 Suspension |
Defect Details | NOT AS PER SPECIFICATION-BALL RACE OD FOUND UNDERSIZE |
1. Problem Description
Defect Description | Ball race OD found undersize |
Detection Stage | Inprocess |
Problem Severity | Safety |
NG Quantity | 1 |
Is Defect Repeatative? | No |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | kasingh@bajajsons.com |
Plant Head/CEO Email ID | crbansal@bajajsons.com |
MD Email ID | sanjay.bajaj@bajajsons.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
600
|
1200
|
300
|
200
|
200
|
2500
|
Check Qty |
600
|
600
|
0
|
200
|
200
|
1600
|
NG Qty |
1
|
0
|
0
|
0
|
0
|
1
|
Scrap | 1 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
All customer end , warehouse, transit & FG stock will re-check for this issue before dispatch to customer. |
3. Process Flow
Process Flow Description |
---|
Pipe cutting-ID Deburring-Flaring-ID. Boring for bush fitting- Bush fitting-Bush welding- Length sizing & countering -CNC Turning-Thread rolling-Grinding 1st- Grinding 2nd- To Assy. |
4. Process Details
Process / Operation | Grinding |
Outsource | No |
Machine / Cell | Centerless Grinding machine |
Machine / Cell No. | CGM-01 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Method | Improper handling of setting part at Grinding machine | During verification found that setting part did not identify after setting,resulting part mixed up w | X |
Tool | Chips stuck on control wheel | During verification found that control wheel dressing done freq. | O |
Man | Unskilled manpower | During verification found that skilled manpower deployed | O |
Method | Improper handling of NG part | During verification found that NG part did not identify | X |
Material | Material hardness less | MTC verified & found ok | O |
Machine | machine Spindle jam | During verification found that machine is ok | O |
6. Inspection Method Analysis (Current)
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
7. Root Cause Analysis (Occurance)
Why 1 | Setting part mix up |
Why 2 | Setting part mix up due to setting part kept at wrong place |
Why 3 | Setting part kept at wrong place due to neglegency of operator |
Why 4 | Neglegency of operator due to lack of awareness |
Why 5 | |
Root Cause (Occurance) | Neglegency of operator due to lack of awareness |
Root Cause Analysis (Outflow)
Why 1 | NG part skipped from inspection stage |
Why 2 | OK part mix up in NG part |
Why 3 | Mix up due to no identified of NG part |
Why 4 | NG part did not identify due to neglegency of checker |
Why 5 | |
Root Cause (Outflow) | NG part did not identify due to neglegency of checker |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Awareness given to machine operator for proper handling of NG part. A special lock type provision will be implement for setting part handling | Vijay Singh | 04/02/2023 | 31/01/2023 | Completed |
Outflow | Awareness given to checker for proper identification of NG part & after identification NG part should be kept in lock & key provision | Sandeep | 31/01/2023 | 30/01/2023 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | NG part will identify & after that part will kept in lock & key provision |
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100 |
10. Evidance of Countermeasure
Occurance (Before) |
NG Part kept at wrong place 346_Occurance_Before.jpg |
Occurance (After) |
NG Part kept at defined place 346_Occurance_After.jpg |
Outflow (Before) |
NG part kept without identification 346_Outflow_Before.jpg |
Outflow (After) |
NG Part identified ang kept in lock & key 346_Outflow_After.jpg |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | Other grinding machines |
12. Document Review
Documents | PFMEA |
Specify Other Document | OPL |
13. Effectiveness Of Action
Reviewed Quantity | 100 |
Reason for submission | Verified next 3 lot and found ok |