QFR No - 8000818063
Defect Details
NC No. 8000818063
NC Date 23/01/2023
NC Submission Date
Part No. F20508007B
Part Name UND BKT SUB-ASSEMBLY (K17B/D)
Supplier Name & Code 100061-BAJAJSONS LIMITED
ETL Plant 1117-ETL K-228/9 Suspension
Defect Details NOT AS PER SPECIFICATION-BALL RACE OD FOUND UNDERSIZE
 
1. Problem Description
Defect Description Ball race OD found undersize
Detection Stage Inprocess
Problem Severity Safety
NG Quantity 1
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID kasingh@bajajsons.com
Plant Head/CEO Email ID crbansal@bajajsons.com
MD Email ID sanjay.bajaj@bajajsons.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
600
1200
300
200
200
2500
Check Qty
600
600
0
200
200
1600
NG Qty
1
0
0
0
0
1
 
Scrap 1
Rework 0
Under Deviation 0
Containment Action
All customer end , warehouse, transit & FG stock will re-check for this issue before dispatch to customer.
 
3. Process Flow
Process Flow Description
Pipe cutting-ID Deburring-Flaring-ID. Boring for bush fitting- Bush fitting-Bush welding- Length sizing & countering -CNC Turning-Thread rolling-Grinding 1st- Grinding 2nd- To Assy.
 
4. Process Details
Process / Operation Grinding
Outsource No
Machine / Cell Centerless Grinding machine
Machine / Cell No. CGM-01
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodImproper handling of setting part at Grinding machineDuring verification found that setting part did not identify after setting,resulting part mixed up wX
ToolChips stuck on control wheelDuring verification found that control wheel dressing done freq.O
ManUnskilled manpowerDuring verification found that skilled manpower deployedO
MethodImproper handling of NG partDuring verification found that NG part did not identifyX
MaterialMaterial hardness lessMTC verified & found okO
Machinemachine Spindle jamDuring verification found that machine is okO
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 Setting part mix up
Why 2 Setting part mix up due to setting part kept at wrong place
Why 3 Setting part kept at wrong place due to neglegency of operator
Why 4 Neglegency of operator due to lack of awareness
Why 5
Root Cause (Occurance) Neglegency of operator due to lack of awareness
 
Root Cause Analysis (Outflow)
Why 1 NG part skipped from inspection stage
Why 2 OK part mix up in NG part
Why 3 Mix up due to no identified of NG part
Why 4 NG part did not identify due to neglegency of checker
Why 5
Root Cause (Outflow) NG part did not identify due to neglegency of checker
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceAwareness given to machine operator for proper handling of NG part. A special lock type provision will be implement for setting part handlingVijay Singh04/02/202331/01/2023Completed
OutflowAwareness given to checker for proper identification of NG part & after identification NG part should be kept in lock & key provisionSandeep31/01/202330/01/2023Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details NG part will identify & after that part will kept in lock & key provision
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100
10. Evidance of Countermeasure
Occurance (Before) NG Part kept at wrong place
346_Occurance_Before.jpg
Occurance (After) NG Part kept at defined place
346_Occurance_After.jpg
Outflow (Before) NG part kept without identification
346_Outflow_Before.jpg
Outflow (After) NG Part identified ang kept in lock & key
346_Outflow_After.jpg
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant Other grinding machines
 
12. Document Review
Documents PFMEA
Specify Other Document OPL
 
13. Effectiveness Of Action
Reviewed Quantity 100
Reason for submission Verified next 3 lot and found ok