QFR No - 8000820735
Defect Details
NC No. 8000820735
NC Date 16/02/2023
NC Submission Date
Part No. 520FZ01902
Part Name HUB CLUTCH K70
Supplier Name & Code 100656-MADHURA DIE CAST PVT.LTD
ETL Plant 1132-ETL K-226/1 TRANSMISSION
Defect Details TAPPING O/SIZE.-CRACK & HEAVY TEPAR MACHINING
 
1. Problem Description
Defect Description Tapper Machining (Dimn 28.2±0.1 mm found up to 27.89~28.48 mm)
Detection Stage Receipt
Problem Severity Fitment
NG Quantity 2
Is Defect Repeatative? No
Defect Sketch / Photo oalbh4q0u5jzjx4ubsgt2ova.jpg
Supplier Communication Details
Quality Head Email ID madhuradiecast@gmail.com
Plant Head/CEO Email ID madhuradiecast@gmail.com
MD Email ID madhuradiecast@gaikegroup.in
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
1000
0
0
500
600
2100
Check Qty
1000
0
0
500
600
2100
NG Qty
2
0
0
1
1
4
 
Scrap 4
Rework 0
Under Deviation 0
Containment Action
1.100% All material segregation at customer end and inhouse end with identification blue marking.
 
3. Process Flow
Process Flow Description
1.Casting 2.fetling 3. CNC 1st Set-up 4.CNC 2nd Set-up 5.Broaching 6.Final Inspection
 
4. Process Details
Process / Operation CNC 2nd Set-up
Outsource No
Machine / Cell CNC
Machine / Cell No. 05
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodComponent was not rest proper in jawCheck and verify possibility component rest inproperX
ManUnskilled operator was operate machineSkill Matrix verify found Level-04 operator operate machineX
ToolJaw loose in runningCheck and verify found okO
MaterialBurr and flash on resting faceFound okO
 
6. Inspection Method Analysis (Current)
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 1:25
7. Root Cause Analysis (Occurance)
Why 1 Tapper Machining (Dimn 28.2±0.1 mm found up to 27.89~28.48 mm)
Why 2 In 2nd side machining Component was not properly resting in jaw.
Why 3 While operator resting the component in the jaw not properly rest.
Why 4
Why 5
Root Cause (Occurance) While operator resting the component in the jaw not properly rest.
 
Root Cause Analysis (Outflow)
Why 1 Inspection done by height gauge
Why 2 Inspection frequency was less
Why 3
Why 4
Why 5
Root Cause (Outflow) Inspection frequency was less
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceAuto loader mechanism is implemented on 2nd side machining stage.Production supervisior15/03/202328/02/2023Completed
Outflow1.Special dial gauge implemented for Taper machining checking 2.Training and awareness given to inspector for checking 100% Taper Machining Checking.QA Supervisor15/03/202328/02/2023Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Started 100% Checking on special dial gauge
Inspection Method Sp. Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 1:1
10. Evidance of Countermeasure
Occurance (Before) Auto loader not available for component resting.
372_Occurance_Before.pdf
Occurance (After) Auto loader mechanism is implemented on 2nd side machining stage.
372_Occurance_After.pdf
Outflow (Before) Taper machining Dim checked by Height gauge
372_Outflow_Before.jpeg
Outflow (After) Taper machining Dim checked by Sp Dial gauge
372_Outflow_After.jpeg
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant NA
 
12. Document Review
Documents PokayokeCheckSheet, InspCheckSheet
Specify Other Document NA
 
13. Effectiveness Of Action
Reviewed Quantity 1000
Reason for submission OK -(Remark-Wrong Defect image upload -Wheel clutch photo upload instead of Hub clutch)