QFR No - 8000821835
Defect Details
NC No. 8000821835
NC Date 25/02/2023
NC Submission Date
Part No. 530MX00812
Part Name STEEL BUSH (FeZn8+ Bight Passivation)
Supplier Name & Code 100106-SHARP ENGINEERS.
ETL Plant 1136-ETL Suspension Sanand
Defect Details DEEP MARK- ID UNCLEAN, ID LINE MARK .
 
1. Problem Description
Defect Description INNER DIA. UNCLEAN SPARIAL MARKS & LINING MARK
Detection Stage Receipt
Problem Severity Fitment
NG Quantity 200
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID quality@apw3.co.in
Plant Head/CEO Email ID kurund.ma@sharp-engineers.com
MD Email ID urkhandelwal@sharp-engineers.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
5000
0
0
0
5000
10000
Check Qty
5000
0
0
0
5000
10000
NG Qty
200
0
0
0
50
250
 
Scrap 0
Rework 150
Under Deviation 0
Containment Action
Segregation done all the pipeline material and WIP.
 
3. Process Flow
Process Flow Description
1) RM Inward inspection 2) 2 Storage 3) Parting and Chamfering 4) Chamfering 5) Plating (Out source) 6) Inward inspection 7) Final Inspection 8) Pre-Dispatch inspection 9) Packing & Dispatch
 
4. Process Details
Process / Operation Purchasing
Outsource Yes
Machine / Cell NA
Machine / Cell No. NA
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MaterialDefective materi i.e. OD line mark/ID line mark/Length& dimensional variation.Inward inspection as per SSPN IS:2500X
ManJudgment error While checkingMaster sample/ Limit sample provided for Checking at final as well as process stageO
MachineInadequate check Point in JH check sheetMonthly JH check sheet available on machine and all the check point is being checked and recorded asO
ToolWrong Tool Insert selectionSOP/WI/CP available on machine and operator aware about it and being followed.O
MethodPart inspection visually as per control plan and inspection check sheetPart are being checked as per control plan and inspection check sheet and record updated.O
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visually
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 1:1
7. Root Cause Analysis (Occurance)
Why 1 Steel Bush ID line mark part reached at ETL
Why 2 RM tube Ø18X12.10 ID line mark itself
Why 3 RM defect
Why 4 NO machining for inner diameter
Why 5 By system design
Root Cause (Occurance) NO machining for inner diameter
 
Root Cause Analysis (Outflow)
Why 1 ID line mark part reached at ETL
Why 2 Inadequate part/defect knowledge to operator/inspector.
Why 3 New defect phenomena
Why 4
Why 5
Root Cause (Outflow) OPL & Q alert not displayed on machine and final inspection stage and Inadequate part/defect knowledge to operator/inspector.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OutflowOPL & Q alert displayed on machine and final inspection stage and training given to all concerns.Mr. Shaikh Laik04/04/202304/04/2023Completed
Occurance100% inspection started after receipt of RM at machining stage, while loading the tube in the machine collet.Mr. Datta Pandhre04/04/202304/04/2023Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details OPL & Q alert displayed on machine and final inspection stage and training given to all concerns.
Inspection Method Other
Other Inspection Method Visually
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 1:1
10. Evidance of Countermeasure
Occurance (Before) Check point not added in the control plan at parting stage .
380_Occurance_Before.jpg
Occurance (After) 100% inspection started after receipt of RM at machining stage while loading the tube in the machine collet.
380_Occurance_After.jpg
Outflow (Before) Check point not evident in CP. OPL & Q alert not displayed on machine and final inspection stage and Inadequate part/defect knowledge to operator/inspector.
380_Outflow_Before.jpg
Outflow (After) Control plan revised and check point added. OPL & Q alert displayed on machine and final inspection stage and training given to all concerns.
380_Outflow_After.jpg
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant STEEL BUSH 312 & 412
 
12. Document Review
Documents ControlPlan, PFMEA, WISOP, InspCheckSheet
Specify Other Document NA
 
13. Effectiveness Of Action
Reviewed Quantity 1
Reason for submission DEEP MARK- ID UNCLEAN, ID LINE MARK