QFR No - 8000825247
Defect Details
NC No. | 8000825247 |
NC Date | 02/04/2023 |
NC Submission Date | |
Part No. | F2HB06910M |
Part Name | OUTER TUBE ANODISED - Ø48 690 SMC |
Supplier Name & Code | 100975-KRISHNA ASSOCIATES |
ETL Plant | 1118-ETL E-92,93 Suspension |
Defect Details | SHADE VARIATION-SHADE VERIATION |
1. Problem Description
Defect Description | Shade variation found on 690 SMC Outer tube |
Detection Stage | Receipt |
Problem Severity | Aesthetic |
NG Quantity | 201 |
Is Defect Repeatative? | No |
Defect Sketch / Photo | 0jb0exe3dv3vs0e5m2na4cnq.jpg |
Supplier Communication Details
Quality Head Email ID | qualitykrishnaassociates01@gmail.com |
Plant Head/CEO Email ID | ravikrishnacoating@gmail.com |
MD Email ID | krishnacoating@gmail.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
201
|
0
|
0
|
0
|
0
|
201
|
Check Qty |
201
|
0
|
0
|
0
|
0
|
201
|
NG Qty |
201
|
0
|
0
|
0
|
0
|
201
|
Scrap | 201 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
checkpoint added in final inspection sheet OPL Displayed at final inspection stage |
3. Process Flow
Process Flow Description |
---|
Pre-treatment - anodizing -Coloring - Sealing- Inspection - packing -Dispatch |
4. Process Details
Process / Operation | Anodizing |
Outsource | No |
Machine / Cell | Anodizing Line |
Machine / Cell No. | 2 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Machine | Faulty timer | cross checked | O |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | Visual |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
7. Root Cause Analysis (Occurance)
Why 1 | Not proper cleaning in water rinse |
Why 2 | Inadequate time in water rinse |
Why 3 | Water rinse timer faulty |
Why 4 | . |
Why 5 | . |
Root Cause (Occurance) | Part not cleaned properly in water rinse tank due to timer of water rinse tank malfunction |
Root Cause Analysis (Outflow)
Why 1 | Defective Sample not displayed at final inspection |
Why 2 | Inspector Not aware about issue |
Why 3 | Checking skipped from inspector |
Why 4 | . |
Why 5 | . |
Root Cause (Outflow) | Defective sample not displayed at final inspection stage, Inspector Not aware about issue |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Timer Controller replaced | Maintenance | 02/04/2023 | 02/04/2023 | Completed |
Outflow | NG part Not displayed at inspection stage | QA | 03/04/2023 | 03/04/2023 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | No |
Change Details | no |
Inspection Method | Other |
Other Inspection Method | OPL Displayed |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
Faulty Timer 397_Occurance_Before.jpg |
Occurance (After) |
Timer changed 397_Occurance_After.jpg |
Outflow (Before) |
Before inspection SOP 397_Outflow_Before.pdf |
Outflow (After) |
Updated Inspection SOP Displayed &
One Point lesson(OPL) Displayed at final inspection stage 397_Outflow_After.pdf |
11. Horizontal Deployment
Horizontal Deployment Required | No |
Applicable Machine / Model / Plant | Timer |
12. Document Review
Documents | PMCheckSheet, InspCheckSheet |
Specify Other Document | OPL |
13. Effectiveness Of Action
Reviewed Quantity | 1600 |
Reason for submission | All part found ok as per requirement |