QFR No - 8000825753
Defect Details
NC No. | 8000825753 |
NC Date | 08/04/2023 |
NC Submission Date | |
Part No. | F2PH02212B |
Part Name | COVER CAP (Ø33 SPD) |
Supplier Name & Code | 100106-SHARP ENGINEERS. |
ETL Plant | 1118-ETL E-92,93 Suspension |
Defect Details | HIGHT U/SIZE.-22 MM DIA UINDER SIZE |
1. Problem Description
Defect Description | HIGHT U/SIZE.-22 MM DIA UINDER SIZE |
Detection Stage | Inprocess |
Problem Severity | Fitment |
NG Quantity | 22 |
Is Defect Repeatative? | No |
Defect Sketch / Photo | 42ckgm3bbcuzzla25ogbxw3a.jpg |
Supplier Communication Details
Quality Head Email ID | quality@sharp-engineers.com |
Plant Head/CEO Email ID | kurund.ma@sharp-engineers.com |
MD Email ID | urkhandelwal@sharp-engineers.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
3000
|
0
|
0
|
500
|
1000
|
4500
|
Check Qty |
3000
|
0
|
0
|
500
|
1000
|
4500
|
NG Qty |
22
|
0
|
0
|
0
|
7
|
29
|
Scrap | 29 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
Segregation done for ETL end Material & FG+WIP material 100% verified. |
3. Process Flow
Process Flow Description |
---|
RM Receipt Inspection & Storage, Blank Cutting & Drilling, Milling, CNC-I, CNC-II, Grinding, Plating, Inward Inspection, Final Inspection, PDI, Packing & Forwarding. |
4. Process Details
Process / Operation | Ist Setup |
Outsource | No |
Machine / Cell | CNC |
Machine / Cell No. | 8 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Tool | Worn Out | Observed Ok | O |
Machine | Machine Parameter variation | Observed OK | O |
Material | - | - | O |
Method | Wrong loading of parts | Observed chips / burr accumulation in jaw | X |
Man | Unskilled | Observed ok | O |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | DVC |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | IS2500.1 |
7. Root Cause Analysis (Occurance)
Why 1 | Wrong loading of parts |
Why 2 | Part position was not OK |
Why 3 | Due to Part resting was incomplete in jaw |
Why 4 | Burr accumulation on Resting face |
Why 5 | Less space for burr removal in V-Jaw |
Root Cause (Occurance) | Burr accumulation on Resting face due to less space for burr/chips removal |
Root Cause Analysis (Outflow)
Why 1 | HEIGHT U/SIZE part observed at customer end |
Why 2 | Not detected during inprocess inspection |
Why 3 | Sample basis inspection with DVC |
Why 4 | Unavailability of gauge |
Why 5 | |
Root Cause (Outflow) | Sample basis inspection with gauge |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | V Jaw are replaced by T Jaw | Mr. Ingole DN | 12/04/2023 | 11/04/2023 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | Length Gauge Implemented |
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | - |
10. Evidance of Countermeasure
Occurance (Before) |
- 405_Occurance_Before.jpg |
Occurance (After) |
- 405_Occurance_After.jpeg |
Outflow (Before) |
- 405_Outflow_Before.xls |
Outflow (After) |
- 405_Outflow_After.jpeg |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | Valve Retainer SPD 31,37 |
12. Document Review
Documents | ControlPlan, PFMEA, InspCheckSheet |
Specify Other Document | - |
13. Effectiveness Of Action
Reviewed Quantity | 8500 |
Reason for submission | All part 22 mm diameter found ok |