QFR No - 8000825772
Defect Details
NC No. | 8000825772 |
NC Date | 07/04/2023 |
NC Submission Date | |
Part No. | F2GN12502B |
Part Name | MAIN SPRING J1A & J1D |
Supplier Name & Code | 101225-HELICAL SPRINGS |
ETL Plant | 1117-ETL K-228/9 Suspension |
Defect Details | NOT AS PER SPECIFICATION-SQUARENESS FOUND NOT OK |
1. Problem Description
Defect Description | Squareness found 2 mm against the spec of 1 mm |
Detection Stage | Receipt |
Problem Severity | Function |
NG Quantity | 483 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | amit.patel@helicalsprings.in |
Plant Head/CEO Email ID | shaikhmoin@helicalsprings.in |
MD Email ID | ataneja@helicalsprings.in |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
6448
|
0
|
0
|
0
|
0
|
6448
|
Check Qty |
6448
|
0
|
0
|
0
|
0
|
6448
|
NG Qty |
448
|
0
|
0
|
0
|
0
|
448
|
Scrap | 0 |
Rework | 100 |
Under Deviation | 0 |
Containment Action |
---|
segregate all material at customer end. |
3. Process Flow
Process Flow Description |
---|
Raw Material > Coiling > Stress Relieving - 1 > End Grinding > Shot peening > Scragging > Length, OD & Wavyness Checking > Stress Relieving -2 > Surface Finish Oiling > PDI > Packing & Dispatch. |
4. Process Details
Process / Operation | Grinding Operation |
Outsource | No |
Machine / Cell | Grinding Machine |
Machine / Cell No. | L4G1 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Method | Grinding Plate Misalignment. | Grinding Plate alignment not checked | X |
Method | Wheel dressing not followed as per defined frequency | Wheel dressing done as per the defined frequency | O |
Material | As per Drawing | RMTC checked found ok | O |
Machine | Herdon | Found ok | O |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | By Spring Standing |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 5 |
7. Root Cause Analysis (Occurance)
Why 1 | End Coil Squareness Out of Spec. |
Why 2 | Spring not loaded straight in Grinding plate |
Why 3 | Grinding plate position not ok |
Why 4 | Holes in layer wise Grinding plates not aligned with respect to each other |
Why 5 | Alignment of holes of three plates checked with insertion of spring |
Root Cause (Occurance) | No robust method to check the alignment of holes of three plates |
Root Cause Analysis (Outflow)
Why 1 | End Coil Squareness Out of Spec. |
Why 2 | Not arrested in inspection |
Why 3 | Inspection done on sampling basis |
Why 4 | No 100% inspection defined |
Why 5 | |
Root Cause (Outflow) | No 100% inspection defined |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Outflow | 100% inspection of springs by making the springs stand on surface | Prod. And Quality | 25/03/2023 | 25/03/2023 | Completed |
Occurance | 1.Alignment of grinding plates holes ensured with the help of rod positioned between grinding plates. [OPL ADDED] 2. Check point of alignment of grinding plates added in grinding setup approval. 3.OPL displayed at Grinding 4.Training provided to the operator and recorded the same | Prod. And Quality | 25/03/2023 | 25/03/2023 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | 100% inspection of springs by making the springs stand on surface |
Inspection Method | Other |
Other Inspection Method | By Spring Standing |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 5 |
10. Evidance of Countermeasure
Occurance (Before) |
Alignment of grinding plates holes ensured with the help of spring insertion in grinding holes 398_Occurance_Before.pdf |
Occurance (After) |
Alignment of grinding plates holes ensured with the help of rod positioned between grinding plates. 398_Occurance_After.pdf |
Outflow (Before) |
Sampling Inspection 398_Outflow_Before.pdf |
Outflow (After) |
100 % inspection by making spring stand 398_Outflow_After.pdf |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | similar model |
12. Document Review
Documents | PFMEA, InspCheckSheet |
Specify Other Document | setup report |
13. Effectiveness Of Action
Reviewed Quantity | 300 |
Reason for submission | Verified next 3 lot and found ok |