QFR No - 8000825878
Defect Details
NC No. | 8000825878 |
NC Date | 10/04/2023 |
NC Submission Date | |
Part No. | B2HF03624O |
Part Name | MCYL PISTON ANODISED-Ø12,K2 FRONT |
Supplier Name & Code | 100505-A B AUTOCOMPONENTS |
ETL Plant | 1120-ETL K-226/2 Disc Brakes |
Defect Details | HIGHT O/SIZE.-EXCESS TIP AT TOP SIDE OF PISTON |
1. Problem Description
Defect Description | Loose ring observed in part |
Detection Stage | Receipt |
Problem Severity | Function |
NG Quantity | 4 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | headqaabauto@gmail.com |
Plant Head/CEO Email ID | kamalabautocomponent@gmail.com |
MD Email ID | abautocomponent@gmail.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
1000
|
0
|
0
|
0
|
2000
|
3000
|
Check Qty |
1000
|
0
|
0
|
0
|
2000
|
3000
|
NG Qty |
4
|
0
|
0
|
0
|
0
|
4
|
Scrap | 4 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
Available 2000nos verified at AB. |
3. Process Flow
Process Flow Description |
---|
RM - Turning - Tip grinding - Inspection - Anodizing - Final inspection - PDIR - Dispatch. |
4. Process Details
Process / Operation | Turning |
Outsource | No |
Machine / Cell | Master Piston Cell |
Machine / Cell No. | Master Piston Cell |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Material | Nil | RM OK as per MTC | O |
Man | No manual intervention in this problem | No manual intervention | O |
Method | Yes | Some parts we are getting | X |
Tool | Nil | Tool ok | O |
Machine | Nil | Machine found ok as per check sheet. | O |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | Visual |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
7. Root Cause Analysis (Occurance)
Why 1 | Tip & Ring found in parts. |
Why 2 | Generating in the process |
Why 3 | |
Why 4 | |
Why 5 | |
Root Cause (Occurance) | Process Problem |
Root Cause Analysis (Outflow)
Why 1 | Tip & Ring found in parts. |
Why 2 | Skipped from the inspection |
Why 3 | New Inspector. |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | New inspector. |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Outflow | 1. Awareness given to the inspectors at final inspection. 2. Defect photos available in defect matrix | Harshith | 22/04/2023 | 22/04/2023 | Completed |
Occurance | 1. Process improvement taken place but still not controlled 100%, 2. Manual tip grinding doing. | Sudhir | 25/04/2023 | 25/04/2023 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | No |
Change Details | Awareness given to inspectors. |
Inspection Method | Other |
Other Inspection Method | Visual |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
|
Occurance (After) |
|
Outflow (Before) |
|
Outflow (After) |
|
11. Horizontal Deployment
Horizontal Deployment Required | |
Applicable Machine / Model / Plant |
12. Document Review
Documents | |
Specify Other Document |
13. Effectiveness Of Action
Reviewed Quantity | |
Reason for submission |