QFR No - 8000827041
Defect Details
NC No. 8000827041
NC Date 22/04/2023
NC Submission Date
Part No. S3GV00112B
Part Name FIX NUT
Supplier Name & Code 100106-SHARP ENGINEERS.
ETL Plant 1116-ETL K-120 Suspension
Defect Details LENGTH UNDERSIZE-WIDTH O/S AND U/S
 
1. Problem Description
Defect Description Total length observed oversize & undersize. This concern repeated many times before.
Detection Stage Receipt
Problem Severity Fitment
NG Quantity 500
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID quality@apw3.co.in
Plant Head/CEO Email ID kurund.ma@sharp-engineers.com
MD Email ID urkhandelwal@sharp-engineers.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
8000
0
0
5000
0
13000
Check Qty
8000
0
0
5000
0
13000
NG Qty
500
0
0
120
0
620
 
Scrap 0
Rework 620
Under Deviation 0
Containment Action
Segregation done immediately for all the ETL and pipeline material.
 
3. Process Flow
Process Flow Description
10) RM Inspection 20) Parting, Forming & Drilling 30) Chamfer Ø 8.10 40) Tapping M8X1.25 6H 50) Semi-finished part inspection 60) Plating process (Outsource) 70) Final Inspection 80) 90) Pre-dispatch inspection 100) Packing and dispatch.
 
4. Process Details
Process / Operation Parting, Forming and Drilling
Outsource Yes
Machine / Cell Traub Machine cell
Machine / Cell No. SE/A/05
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MaterialIncorrect RM gradeThird part inspection verified for chemical composition and hardness testing as per requirement.O
MethodWrong checking method/sample size.Checking done by SESG for sampling basis inspection as per IS:2500O
ToolTool worn outTool life for all the tool i.e. forming tool, drill, tap and insert are not defined & not recorded.X
ManUn-skilled OperatorStage wise skill matrix and operator license ar evident as per F/HR/06O
MachineInadequate check Point in JH check sheetMonthly JH check sheet available on machine and all the check point is being checked and recorded asO
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 1:1
7. Root Cause Analysis (Occurance)
Why 1 DIM 15.0+/-0.1 OVER SIZE.
Why 2 Parting tool worn out.
Why 3 Parting tool worn out earlier than defined frequency 300/sharpening
Why 4 Tool life not getting as per defined tool life
Why 5 Coolant concentration is not being monitored.
Root Cause (Occurance) Parting tool worn out earlier than defined frequency 300/sharpening, because coolant concentration is not being monitored.
 
Root Cause Analysis (Outflow)
Why 1 DIM. 15.0+/-0.1 over size part reached at ETL
Why 2 Not detected at final inspection stage.
Why 3 Sampling basis inspection as per IS 2500
Why 4 Sample size defined by system.
Why 5
Root Cause (Outflow) Sampling basis inspection as per IS:2500, No 100% inspection for Total length 15.0+/-0.1mm
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceTool life re-defined 200/sharpening for parting tool and being monitored as per F/PROD/07. on job training given to operator as per F/HR/05Mr. Datta Pandhre03/05/202303/05/2023Completed
Outflow100% inspection started as per revised control plan and checking is being done by SESG for inspection. OPL displayed at final inspection stage and on job training given to operator.Mr. Shaikh L.N.03/05/202303/05/2023Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 100% inspection started for dimension 15.0+/-0.1mm
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 1:1
10. Evidance of Countermeasure
Occurance (Before) Parting tool worn out earlier than defined frequency 300/sharpening, because coolant concentration is not being monitored.
432_Occurance_Before.jpg
Occurance (After) Tool life re-defined 200/sharpening for parting tool and being monitored as per F/PROD/07. on job training given to operator as per F/HR/05
432_Occurance_After.jpg
Outflow (Before) Sampling basis inspection as per IS:2500, No 100% inspection for Total length 15.0+/-0.1mm
432_Outflow_Before.jpg
Outflow (After) 100% inspection started as per revised control plan and checking is being done by SESG for inspection. OPL displayed at final inspection stage and on job training given to operator.
432_Outflow_After.jpg
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant FIX NUT (Pulsar Model) part number (520DU00102)
 
12. Document Review
Documents ControlPlan, PFMEA, WISOP, InspCheckSheet
Specify Other Document NA
 
13. Effectiveness Of Action
Reviewed Quantity 10
Reason for submission Corrective action parts submission.