QFR No - 8000827285
Defect Details
NC No. 8000827285
NC Date 24/04/2023
NC Submission Date
Part No. 520HL00202
Part Name OIL LOCK COLLAR
Supplier Name & Code 100106-SHARP ENGINEERS.
ETL Plant 1146-ETL Suspension Narasapura
Defect Details HIGHT U/SIZE.-TOTAL LENGHT LESS
 
1. Problem Description
Defect Description Oil lock collar total length less issue
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 12
Is Defect Repeatative? No
Defect Sketch / Photo e01cj5hc5pkgorczc3ywsn10.xlsx
Supplier Communication Details
Quality Head Email ID quality@apw3.co.in
Plant Head/CEO Email ID kurund.ma@sharp-engineers.com
MD Email ID urkhandelwal@sharp-engineers.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
5000
5000
0
2000
0
12000
Check Qty
5000
5000
0
2000
0
12000
NG Qty
12
0
0
1
0
13
 
Scrap 13
Rework 0
Under Deviation 0
Containment Action
Segregation done at ETL and in-house FG stock for to avoid further difficulties.
 
3. Process Flow
Process Flow Description
1) RM inward inspection 2) Parting and chamfering 3) CNC 1st 4) Plating process (outsource-Pranav coating) 5) Inward inspection 6) Storage 7) Final Inspection 8) Pre-dispatch Inspection 9) Packing & forwarding
 
4. Process Details
Process / Operation CNC 1st
Outsource No
Machine / Cell CNC Machine Shop
Machine / Cell No. SE/CNC/03
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodChecking method by attribute type height gaugeChecking done by vernier caliperX
MaterialInput material under sizeYes, input material observed under sizeX
MachineInadequate check Point in JH check sheetMonthly JH check sheet available on machine and all the check point is being checked and recorded asO
ToolParting tool and insert worn outTool life for all the tool i.e. parting tool and insert are defined and recorded as per F/PROD/07O
ManUn-skilled OperatorStage wise skill matrix and operator license are evident as per F/HR/06O
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 1:1
7. Root Cause Analysis (Occurance)
Why 1 HIGHT U/SIZE.-TOTAL LENGHT LESS
Why 2 INPUT MATERIAL OF CNC MACHINE UNDER SIZE
Why 3 TAPER OBSERVED IN THE INPUT PART
Why 4 INCOREECT TOOL SETTING BY NEW OPERATOR
Why 5 STAGE WISE SKILL MATRIX NOT FOLLOWED. SEMI-SKILLED OPERATOR.
Root Cause (Occurance) STAGE WISE SKILL MATRIX NOT FOLLOWED. SEMI-SKILLED OPERATOR. AND TRAINING NOT GIVEN TO OPERATOR.
 
Root Cause Analysis (Outflow)
Why 1 HIGHT U/SIZE.-TOTAL LENGHT LESS
Why 2 SAMPLING BASIS INSPECTION AS PER IS:2500 BY VERNIER CALIPER
Why 3 NO 100% INSPECTION BY ATTRIBUTE TYPE GAUGE
Why 4 CHECKING METHOD DEFINED BY SYSTEM
Why 5
Root Cause (Outflow) INSPECTION DONE BY SAMPLING BASIS AS PER IS:2500, 100% INSPECTION NOT DONE
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceSTAGE WISE SKILL MATRIX UPDATED AND TRAINING GIVEN TO OPERATOR, AND OPERATOR DEFINED AS PER SKILL REQUIREMENT.MR. DATTA PANDHRE03/05/202303/05/2023Completed
OutflowINSPECTION STARTED 100% BY ATTRIBUTE TYPE GAUGE AND CONTROL PLAN UPDATEDMR, SHAIKH LAIK03/05/202303/05/2023Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details INSPECTION STARTED BY ATTRIBUTE TYPE GAUGE IN PLACE OF VERNIER CALIPER.
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 1:1
10. Evidance of Countermeasure
Occurance (Before) STAGE WISE SKILL MATRIX NOT FOLLOWED. SEMI-SKILLED OPERATOR. AND TRAINING NOT GIVEN TO OPERATOR.
426_Occurance_Before.jpg
Occurance (After) STAGE WISE SKILL MATRIX UPDATED AND TRAINING GIVEN TO OPERATOR, AND OPERATOR DEFINED AS PER SKILL REQUIREMENT.
426_Occurance_After.jpg
Outflow (Before) NO 100% INSPECTION BY ATTRIBUTE TYPE GAUGE
426_Outflow_Before.jpg
Outflow (After) INSPECTION STARTED 100% BY ATTRIBUTE TYPE GAUGE AND CONTROL PLAN UPDATED
426_Outflow_After.jpg
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant OIL LOCK COLLAR K-60
 
12. Document Review
Documents ControlPlan, PFMEA, WISOP, InspCheckSheet
Specify Other Document NA
 
13. Effectiveness Of Action
Reviewed Quantity 500
Reason for submission Reviewed 500 no`s found ok