QFR No - 8000827285
Defect Details
NC No. | 8000827285 |
NC Date | 24/04/2023 |
NC Submission Date | |
Part No. | 520HL00202 |
Part Name | OIL LOCK COLLAR |
Supplier Name & Code | 100106-SHARP ENGINEERS. |
ETL Plant | 1146-ETL Suspension Narasapura |
Defect Details | HIGHT U/SIZE.-TOTAL LENGHT LESS |
1. Problem Description
Defect Description | Oil lock collar total length less issue |
Detection Stage | Inprocess |
Problem Severity | Fitment |
NG Quantity | 12 |
Is Defect Repeatative? | No |
Defect Sketch / Photo | e01cj5hc5pkgorczc3ywsn10.xlsx |
Supplier Communication Details
Quality Head Email ID | quality@apw3.co.in |
Plant Head/CEO Email ID | kurund.ma@sharp-engineers.com |
MD Email ID | urkhandelwal@sharp-engineers.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
5000
|
5000
|
0
|
2000
|
0
|
12000
|
Check Qty |
5000
|
5000
|
0
|
2000
|
0
|
12000
|
NG Qty |
12
|
0
|
0
|
1
|
0
|
13
|
Scrap | 13 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
Segregation done at ETL and in-house FG stock for to avoid further difficulties. |
3. Process Flow
Process Flow Description |
---|
1) RM inward inspection 2) Parting and chamfering 3) CNC 1st 4) Plating process (outsource-Pranav coating) 5) Inward inspection 6) Storage 7) Final Inspection 8) Pre-dispatch Inspection 9) Packing & forwarding |
4. Process Details
Process / Operation | CNC 1st |
Outsource | No |
Machine / Cell | CNC Machine Shop |
Machine / Cell No. | SE/CNC/03 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Method | Checking method by attribute type height gauge | Checking done by vernier caliper | X |
Material | Input material under size | Yes, input material observed under size | X |
Machine | Inadequate check Point in JH check sheet | Monthly JH check sheet available on machine and all the check point is being checked and recorded as | O |
Tool | Parting tool and insert worn out | Tool life for all the tool i.e. parting tool and insert are defined and recorded as per F/PROD/07 | O |
Man | Un-skilled Operator | Stage wise skill matrix and operator license are evident as per F/HR/06 | O |
6. Inspection Method Analysis (Current)
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 1:1 |
7. Root Cause Analysis (Occurance)
Why 1 | HIGHT U/SIZE.-TOTAL LENGHT LESS |
Why 2 | INPUT MATERIAL OF CNC MACHINE UNDER SIZE |
Why 3 | TAPER OBSERVED IN THE INPUT PART |
Why 4 | INCOREECT TOOL SETTING BY NEW OPERATOR |
Why 5 | STAGE WISE SKILL MATRIX NOT FOLLOWED. SEMI-SKILLED OPERATOR. |
Root Cause (Occurance) | STAGE WISE SKILL MATRIX NOT FOLLOWED. SEMI-SKILLED OPERATOR. AND TRAINING NOT GIVEN TO OPERATOR. |
Root Cause Analysis (Outflow)
Why 1 | HIGHT U/SIZE.-TOTAL LENGHT LESS |
Why 2 | SAMPLING BASIS INSPECTION AS PER IS:2500 BY VERNIER CALIPER |
Why 3 | NO 100% INSPECTION BY ATTRIBUTE TYPE GAUGE |
Why 4 | CHECKING METHOD DEFINED BY SYSTEM |
Why 5 | |
Root Cause (Outflow) | INSPECTION DONE BY SAMPLING BASIS AS PER IS:2500, 100% INSPECTION NOT DONE |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | STAGE WISE SKILL MATRIX UPDATED AND TRAINING GIVEN TO OPERATOR, AND OPERATOR DEFINED AS PER SKILL REQUIREMENT. | MR. DATTA PANDHRE | 03/05/2023 | 03/05/2023 | Completed |
Outflow | INSPECTION STARTED 100% BY ATTRIBUTE TYPE GAUGE AND CONTROL PLAN UPDATED | MR, SHAIKH LAIK | 03/05/2023 | 03/05/2023 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | INSPECTION STARTED BY ATTRIBUTE TYPE GAUGE IN PLACE OF VERNIER CALIPER. |
Inspection Method | Instrument |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 1:1 |
10. Evidance of Countermeasure
Occurance (Before) |
STAGE WISE SKILL MATRIX NOT FOLLOWED. SEMI-SKILLED OPERATOR. AND TRAINING NOT GIVEN TO OPERATOR. 426_Occurance_Before.jpg |
Occurance (After) |
STAGE WISE SKILL MATRIX UPDATED AND TRAINING GIVEN TO OPERATOR, AND OPERATOR DEFINED AS PER SKILL REQUIREMENT. 426_Occurance_After.jpg |
Outflow (Before) |
NO 100% INSPECTION BY ATTRIBUTE TYPE GAUGE 426_Outflow_Before.jpg |
Outflow (After) |
INSPECTION STARTED 100% BY ATTRIBUTE TYPE GAUGE AND CONTROL PLAN UPDATED 426_Outflow_After.jpg |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | OIL LOCK COLLAR K-60 |
12. Document Review
Documents | ControlPlan, PFMEA, WISOP, InspCheckSheet |
Specify Other Document | NA |
13. Effectiveness Of Action
Reviewed Quantity | 500 |
Reason for submission | Reviewed 500 no`s found ok |