QFR No - 8000827286
Defect Details
NC No. | 8000827286 |
NC Date | 24/04/2023 |
NC Submission Date | |
Part No. | 520HL00202 |
Part Name | OIL LOCK COLLAR |
Supplier Name & Code | 100097-MAHAVIR INDUSTRIES |
ETL Plant | 1146-ETL Suspension Narasapura |
Defect Details | LENGTH UNDERSIZE-TOTAL LENGHT LESS |
1. Problem Description
Defect Description | Oil lock collar total length less issue |
Detection Stage | Inprocess |
Problem Severity | Fitment |
NG Quantity | 10 |
Is Defect Repeatative? | No |
Defect Sketch / Photo | e01cj5hc5pkgorczc3ywsn10.xlsx |
Supplier Communication Details
Quality Head Email ID | quality@mahavirind.co.in |
Plant Head/CEO Email ID | production@mahavirind.co.in |
MD Email ID | rajesh@mahavirind.co.in |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
3000
|
0
|
0
|
1800
|
0
|
4800
|
Check Qty |
3000
|
0
|
0
|
0
|
0
|
3000
|
NG Qty |
10
|
0
|
0
|
0
|
0
|
10
|
Scrap | 10 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
All material Customer End and Mahavir Ind. RFD Material verified. |
3. Process Flow
Process Flow Description |
---|
RM Inward- store- Traub parting- OD Grinding - Plating - Final Inspection- Packing -Transport |
4. Process Details
Process / Operation | Traub parting |
Outsource | Yes |
Machine / Cell | Traub Cutting |
Machine / Cell No. | Traub No.2 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Machine | Bend Pipe | Bend Pipe not Movement as per Required Length due to Balance Weight Improper. | X |
6. Inspection Method Analysis (Current)
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 100 |
7. Root Cause Analysis (Occurance)
Why 1 | Length Under Size |
Why 2 | Bend Pipe Not movement during the parting Process on Traub machine |
Why 3 | Weight Balancing Not enough. |
Why 4 | |
Why 5 | |
Root Cause (Occurance) | Weight Balancing Not enough. |
Root Cause Analysis (Outflow)
Why 1 | Length Under Size |
Why 2 | Defected material skipped by Inspector During Final inspection |
Why 3 | Final Inspection sampling frequency low |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | Final Inspection sampling frequency low |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Required Balancing weight Increase for bend pipe movement. | Mr.Suresh Kapgate/ Mr. Pralhad Bhawar | 27/04/2023 | Pending |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | 1) Sampling Size Increase .2) Length Gauge Provide On Traub Machine . |
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
Parting Pipe Not proper movement On Traub Due to Weight Balancing Improper 424_Occurance_Before.xlsx |
Occurance (After) |
As per Required Balancing Weight Increase for bend pipe Parting 424_Occurance_After.xlsx |
Outflow (Before) |
Length gauge not available on Traub Machine. 424_Outflow_Before.xlsx |
Outflow (After) |
Length gauge Provide On Parting Process Traub Machine 424_Outflow_After.xlsx |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | For All Oil lock collars Weight Balancer Increase |
12. Document Review
Documents | ControlPlan, PFMEA |
Specify Other Document | no |
13. Effectiveness Of Action
Reviewed Quantity | |
Reason for submission |