QFR No - 8000827592
Defect Details
NC No. 8000827592
NC Date 26/04/2023
NC Submission Date
Part No. F1LG00902B
Part Name SEAT PIPE -K86A
Supplier Name & Code 100538-NARINDER PARKASH AND CO
ETL Plant 1146-ETL Suspension Narasapura
Defect Details LENGTH UNDERSIZE-TOTAL LENGHT LESS
 
1. Problem Description
Defect Description Seat pipe total length less issue
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 2
Is Defect Repeatative? Yes
Defect Sketch / Photo myxhb1uoyxroq2e4tssk4rhv.jpg
Supplier Communication Details
Quality Head Email ID quality@npcindustries.in
Plant Head/CEO Email ID anand@npcindustries.in
MD Email ID ajay@npcindustries.in
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
4000
0
0
2000
0
6000
Check Qty
4000
0
0
4
0
4004
NG Qty
2
0
0
4
0
6
 
Scrap 6
Rework 0
Under Deviation 0
Containment Action
Segregated all parts at ETL, at Warehouse & at NPC Nabha.
 
3. Process Flow
Process Flow Description
1.Raw Material 2.Cutting & Chamfering 3. Multistation Draw 4.Head Formation 5.Rough Grinding 6.Punching 7.CNC Head Turning 8.CNC Boring & Facing 9.Tapping 10. Chamfering 1&2 11.Finish Grinding 12.Final Inspection 13.Cleaning 14.Oiling 15.Packing & Dispatch
 
4. Process Details
Process / Operation CNC Boring
Outsource No
Machine / Cell CNC
Machine / Cell No. CNC-04
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MaterialMaterial hardness less/moreAfter verification we found material Hardness as per spec.O
MethodOther model mixed during processingafter verification We found material was ok.O
MachineCnc Program was tamperedAfter verification we found CNC program was ok as per drawing.O
Methodvernier not calibratedafter Verification vernier was CalibratedO
MethodMaterial clamping method inadequateAfter verification we found material clamping method inadequate.X
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection No
Checking Freq. Sampling
Sampling No
Sample Size as per CP
7. Root Cause Analysis (Occurance)
Why 1 seatpipe total length Less
Why 2 seat pipe did not proper fit in collet.
Why 3 Part did not clamp as per requirement.
Why 4 Chips stucked with stopper pin
Why 5 no proper cleaning during operation
Root Cause (Occurance) no proper cleaning during operation
 
Root Cause Analysis (Outflow)
Why 1 seatpipe total length Less
Why 2 Could not be detected at final inspection
Why 3 Skipped in Sampling at Final Inspection
Why 4 Sampling quantity was less
Why 5
Root Cause (Outflow) Sampling quantity was less
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
Outflow100% inspection during final inspectionMr. Ankush29/04/202328/04/2023Completed
Occurancefreezed cleaning frequency by Air gun during operation.Mr. Gurpreet Singh29/04/202328/04/2023Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 100% Inspection During final inspection.
Inspection Method Other
Other Inspection Method Use Flat plate
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Chips stucked with stopper
433_Occurance_Before.jpeg
Occurance (After) freezed cleaning frequency by Air gun during operation.
433_Occurance_After.jpeg
Outflow (Before) We checked with sampling inspection By Digital vernier
433_Outflow_Before.jpeg
Outflow (After) Increase sampling quantity at work station & use of surface flat for length checking at final inspection
433_Outflow_After.png
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant CNC Machine
 
12. Document Review
Documents ControlPlan, PFMEA, WISOP, InspCheckSheet
Specify Other Document No
 
13. Effectiveness Of Action
Reviewed Quantity 2000
Reason for submission Reviewed 2000 no`s found ok