QFR No - 8000827660
Defect Details
NC No. 8000827660
NC Date 26/04/2023
NC Submission Date
Part No. 5230103200
Part Name THROTTLE CONTROL PULLY FOR H BAR ASSLY
Supplier Name & Code 101086-PUNE POLYMERS PVT. LTD.
ETL Plant 1102-ETL L-6 Die Casting
Defect Details FITTMENT NOT OK.-ID 21.95 UNDERSIZE
 
1. Problem Description
Defect Description Fitment ID dia 21.95 undersize . Spec 21.95 observed 21.7. to 21.80
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 42
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID qa.waluj@punepolymers.com
Plant Head/CEO Email ID planthead.waluj@punepolymers.com
MD Email ID s.gupta@punepolymers.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
3000
0
0
0
5000
8000
Check Qty
3000
0
0
0
5000
8000
NG Qty
0
0
0
0
300
300
 
Scrap 0
Rework 300
Under Deviation 0
Containment Action
100 % inspection with gauge & green marking for confirmation.
 
3. Process Flow
Process Flow Description
Receipt - Injection molding - Annealing - De-flashing -Inspection
 
4. Process Details
Process / Operation Injection molding
Outsource No
Machine / Cell Injection mold shop
Machine / Cell No. IM 100T
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ToolLess dia of punch in mold22.04 mm against requirement of 22.20 mmO
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method DVC
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 10 Nos
7. Root Cause Analysis (Occurance)
Why 1 Fitment issue
Why 2 ID undersize.
Why 3 Punch dia less (22.04 mm) in the mold.
Why 4
Why 5
Root Cause (Occurance) Punch dia less (22.04 mm) in the mold.
 
Root Cause Analysis (Outflow)
Why 1 Fitment issue
Why 2 ID undersize.
Why 3 Not detected in sampling.
Why 4
Why 5
Root Cause (Outflow) Not detected in sampling.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceNew punch with increased dia of 22.20 mm replaced to meet ID dimensions as per specification 21.95 ± 0.1 mm.Balu Kasbe25/05/2023Inprocess
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Inspection by Plug gauge instead of DVC
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100 %
10. Evidance of Countermeasure
Occurance (Before) Punch dia less (22.04 mm) in the mold.
439_Occurance_Before.xlsx
Occurance (After) New punch with increased dia of 22.20 mm replaced to meet ID dimensions as per specification 21.95 ± 0.1 mm.
439_Occurance_After.xlsx
Outflow (Before) Not detected in sampling.
439_Outflow_Before.xlsx
Outflow (After) 100 % inspection of part by QA inspector by "GO" "NOGO" plug gauge before thread weaving of part & green marking for confirmation.
439_Outflow_After.xlsx
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant Throttle control pulley 24191101
 
12. Document Review
Documents PMCheckSheet, PFMEA, InspCheckSheet
Specify Other Document NA
 
13. Effectiveness Of Action
Reviewed Quantity
Reason for submission