QFR No - 8000827791
Defect Details
NC No. | 8000827791 |
NC Date | 28/04/2023 |
NC Submission Date | |
Part No. | F2PH00902B |
Part Name | VALVE RETAINER (C101B) |
Supplier Name & Code | 101255-MAHAVIR INDUSTRIES |
ETL Plant | 1146-ETL Suspension Narasapura |
Defect Details | RUSTY-RUST ISSUE |
1. Problem Description
Defect Description | valve retainer rust issue |
Detection Stage | Receipt |
Problem Severity | Aesthetic |
NG Quantity | 1000 |
Is Defect Repeatative? | No |
Defect Sketch / Photo | hu2g3xnwwdoxzi2mq5cqmlnm.jpg |
Supplier Communication Details
Quality Head Email ID | quality@mahavirind.co.in |
Plant Head/CEO Email ID | production@mahavirind.co.in |
MD Email ID |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
6000
|
6000
|
0
|
0
|
0
|
12000
|
Check Qty |
6000
|
6000
|
0
|
0
|
0
|
12000
|
NG Qty |
1000
|
0
|
0
|
0
|
0
|
1000
|
Scrap | 1000 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
All Material Check at the Customer End and Warehouse End. |
3. Process Flow
Process Flow Description |
---|
RM inward - store - Parting - Semi finish Inward - CNC ( Counter ID Machining ) - OD Grinding- Plating - Final Inspection - Packing - Dispatch - Transport- warehouse- Customer Received |
4. Process Details
Process / Operation | Warehouse Loading - Unloading Handling Problem |
Outsource | No |
Machine / Cell | Narsapura Warehouse |
Machine / Cell No. | Narsapura Warehouse |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | Visual |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
7. Root Cause Analysis (Occurance)
Why 1 | Rusty |
Why 2 | Finish Good Material Wet at warehouse |
Why 3 | Finish Good Lying On Shop floor |
Why 4 | Packing Bag Torn of finish good |
Why 5 | Improper Material Handling |
Root Cause (Occurance) | Packing Bag Torn of finish good |
Root Cause Analysis (Outflow)
Why 1 | Rusty |
Why 2 | Finish Good Material More No. of days lying at transport Godown |
Why 3 | Inform To godown person |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | Finish Good Material More No. of days lying at transport Godown |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | 1)Improper Material Handling .2)Finish Good Material More No. of days lying at transport Godown | Mahavir QA | 10/05/2023 | 10/05/2023 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | 1)Packing as per Customer Standards. 2) HDPE white, Heavy thickness and clean Gunny bags use for outer coating packing. |
Inspection Method | Other |
Other Inspection Method | Packing Visual Obs |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100 |
10. Evidance of Countermeasure
Occurance (Before) |
1)Finish Good Packing Bag Torn at warehouse during Material Handling .
2)Low Thickness Poly Bag. 443_Occurance_Before.xlsx |
Occurance (After) |
1)Inner poly bag thickness increases up to 400 gauge Instead of 300 Gauge for Tearing problems avoid Suitable to Material Handling. 2)HDPE white , Heavy thickness and clean Gunny bags use for outer coating packing. 443_Occurance_After.xlsx |
Outflow (Before) |
Finish Good Material More No. of days lying at transport godown 443_Outflow_Before.jpg |
Outflow (After) |
As per the attached packing standard 443_Outflow_After.xlsx |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | Applicable all Narsapur-supplied Parts |
12. Document Review
Documents | PackingStd |
Specify Other Document | No |
13. Effectiveness Of Action
Reviewed Quantity | 1000 |
Reason for submission | Reviewed 1000 no`s found ok |