QFR No - 8000827812
Defect Details
NC No. | 8000827812 |
NC Date | 28/04/2023 |
NC Submission Date | |
Part No. | S3GD01938B |
Part Name | INNER TUBE BALL PASSED-TVS KING REAR |
Supplier Name & Code | 100876-ACCRETE ELECTROMECH PVT.LTD. |
ETL Plant | 1116-ETL K-120 Suspension |
Defect Details | STREGHTNESS NOT OK-STREGHTNESS NOT OK |
1. Problem Description
Defect Description | Straightness not Ok concern observed. |
Detection Stage | Receipt |
Problem Severity | Fitment |
NG Quantity | 507 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | qahead@accrete.in |
Plant Head/CEO Email ID | ppc@accrete.in |
MD Email ID | damodani@accrete.in |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
3000
|
0
|
0
|
800
|
0
|
3800
|
Check Qty |
3000
|
0
|
0
|
800
|
0
|
3800
|
NG Qty |
507
|
0
|
0
|
100
|
0
|
607
|
Scrap | 607 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
100% inspection done for inner diameter at ETL as well as AEPL end. |
3. Process Flow
Process Flow Description |
---|
1. Raw tube receipt 2. Tube cutting 3. Washing 4. Tube chamfering 5. Dispatch |
4. Process Details
Process / Operation | Raw material |
Outsource | Yes |
Machine / Cell | NA |
Machine / Cell No. | NA |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Material | RM tube defect | RM tube defect | O |
6. Inspection Method Analysis (Current)
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 10 nos |
7. Root Cause Analysis (Occurance)
Why 1 | Straightness not ok issue observed |
Why 2 | RM Defect |
Why 3 | |
Why 4 | |
Why 5 | |
Root Cause (Occurance) | RM Defect (Communicated with supplier) |
Root Cause Analysis (Outflow)
Why 1 | Straightness not ok issue observed |
Why 2 | Straightness not inspected at AEPL |
Why 3 | 100 percent inspection not performed |
Why 4 | ID Straightness inspected on sample basis |
Why 5 | |
Root Cause (Outflow) | ID Straightness inspected on sample basis |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Outflow | 100% inspection started with straightness gauge before dispatch | Prakash ade | 03/05/2023 | 03/05/2023 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | 100% inspection with straightness gauge started |
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
Not applicable 441_Occurance_Before.xlsx |
Occurance (After) |
Not applicable 441_Occurance_After.xlsx |
Outflow (Before) |
SOP of SOCO cutting machine does not contain straightness parameter. 441_Outflow_Before.xlsx |
Outflow (After) |
SOP of SOCO cutting machine updated and straightness inspection added in it. 441_Outflow_After.xlsx |
11. Horizontal Deployment
Horizontal Deployment Required | No |
Applicable Machine / Model / Plant | Not applicable |
12. Document Review
Documents | WISOP, InspCheckSheet |
Specify Other Document | OPL |
13. Effectiveness Of Action
Reviewed Quantity | 10 |
Reason for submission | Corrective action parts submission. |