QFR No - 8000827812
Defect Details
NC No. 8000827812
NC Date 28/04/2023
NC Submission Date
Part No. S3GD01938B
Part Name INNER TUBE BALL PASSED-TVS KING REAR
Supplier Name & Code 100876-ACCRETE ELECTROMECH PVT.LTD.
ETL Plant 1116-ETL K-120 Suspension
Defect Details STREGHTNESS NOT OK-STREGHTNESS NOT OK
 
1. Problem Description
Defect Description Straightness not Ok concern observed.
Detection Stage Receipt
Problem Severity Fitment
NG Quantity 507
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID qahead@accrete.in
Plant Head/CEO Email ID ppc@accrete.in
MD Email ID damodani@accrete.in
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
3000
0
0
800
0
3800
Check Qty
3000
0
0
800
0
3800
NG Qty
507
0
0
100
0
607
 
Scrap 607
Rework 0
Under Deviation 0
Containment Action
100% inspection done for inner diameter at ETL as well as AEPL end.
 
3. Process Flow
Process Flow Description
1. Raw tube receipt 2. Tube cutting 3. Washing 4. Tube chamfering 5. Dispatch
 
4. Process Details
Process / Operation Raw material
Outsource Yes
Machine / Cell NA
Machine / Cell No. NA
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MaterialRM tube defectRM tube defectO
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 10 nos
7. Root Cause Analysis (Occurance)
Why 1 Straightness not ok issue observed
Why 2 RM Defect
Why 3
Why 4
Why 5
Root Cause (Occurance) RM Defect (Communicated with supplier)
 
Root Cause Analysis (Outflow)
Why 1 Straightness not ok issue observed
Why 2 Straightness not inspected at AEPL
Why 3 100 percent inspection not performed
Why 4 ID Straightness inspected on sample basis
Why 5
Root Cause (Outflow) ID Straightness inspected on sample basis
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
Outflow100% inspection started with straightness gauge before dispatchPrakash ade03/05/202303/05/2023Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 100% inspection with straightness gauge started
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Not applicable
441_Occurance_Before.xlsx
Occurance (After) Not applicable
441_Occurance_After.xlsx
Outflow (Before) SOP of SOCO cutting machine does not contain straightness parameter.
441_Outflow_Before.xlsx
Outflow (After) SOP of SOCO cutting machine updated and straightness inspection added in it.
441_Outflow_After.xlsx
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant Not applicable
 
12. Document Review
Documents WISOP, InspCheckSheet
Specify Other Document OPL
 
13. Effectiveness Of Action
Reviewed Quantity 10
Reason for submission Corrective action parts submission.