QFR No - 8000831090
Defect Details
NC No. | 8000831090 |
NC Date | 31/05/2023 |
NC Submission Date | |
Part No. | B2FP01013O |
Part Name | HOLDER BRACKET FINISHED - REML |
Supplier Name & Code | 100398-MANOJ INDUSTRIES |
ETL Plant | 1120-ETL K-226/2 Disc Brakes |
Defect Details | DAMAGES-AFTER 100% INSP. BH,PINHOLES,DENT,DAMAGE |
1. Problem Description
Defect Description | Dent, & Blow holes observed on parts |
Detection Stage | Receipt |
Problem Severity | Aesthetic |
NG Quantity | 25 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | qad@manojindustrieskop.com |
Plant Head/CEO Email ID | foundry@manojindustrieskop.com |
MD Email ID | mgnt@manojindustrieskop.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
1750
|
450
|
0
|
500
|
0
|
2700
|
Check Qty |
1750
|
450
|
0
|
500
|
0
|
2700
|
NG Qty |
18
|
13
|
0
|
7
|
0
|
38
|
Scrap | 38 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
100% visual Inspection of All pipeline stock |
3. Process Flow
Process Flow Description |
---|
casting ,VMC machining ,Slotting ,Final Inspection |
4. Process Details
Process / Operation | casting ,VMC machining |
Outsource | No |
Machine / Cell | ENDURANCE CELL |
Machine / Cell No. | VMC-14 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | visual Inspection |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
7. Root Cause Analysis (Occurance)
Why 1 | Dent damage observed on casting |
Why 2 | Casting dent observed at parting process |
Why 3 | After parting parts not kept properly |
Why 4 | operator keeps the parts in open bin from 2ft height |
Why 5 | |
Root Cause (Occurance) | operator keeps the parts in open bin from 2ft height |
Root Cause Analysis (Outflow)
Why 1 | Dent damage observed on casting |
Why 2 | skipped from final inspector |
Why 3 | |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | skipped from final inspector |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|
9. Inspection Method After Customer Complaint
Change In Inspection System | No |
Change Details | No |
Inspection Method | Other |
Other Inspection Method | Visual Inspection |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
After parting operation parts kept in open bin 456_Occurance_Before.png |
Occurance (After) |
After parting parts kept in partitioned bin 456_Occurance_After.jpg |
Outflow (Before) |
no Dot mark provided 456_Outflow_Before.jpg |
Outflow (After) |
Dot mark provided 456_Outflow_After.jpg |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | Master cylinder,Calipers |
12. Document Review
Documents | WISOP |
Specify Other Document | Quality plan |
13. Effectiveness Of Action
Reviewed Quantity | 100 |
Reason for submission | NO damage observed in corrected lot |