QFR No - 8000831275
Defect Details
NC No. 8000831275
NC Date 01/06/2023
NC Submission Date
Part No. S1AB00612B
Part Name ADJUSTER PLATED
Supplier Name & Code 100782-NICE STEEL INDUSTRIES
ETL Plant 1146-ETL Suspension Narasapura
Defect Details WELDING NOT OK-IMPROPER WELDING (GAP) , EXTRA WELDING P
 
1. Problem Description
Defect Description adjuster welding issues (improper welding (gap ) )
Detection Stage Receipt
Problem Severity Safety
NG Quantity 6036
Is Defect Repeatative? No
Defect Sketch / Photo 25w4rf2t3qmac05lbmkjdpe3.gif
Supplier Communication Details
Quality Head Email ID ppc.nice@batragroup.biz
Plant Head/CEO Email ID ho.nice@batragroup.biz
MD Email ID hitesh@batragroup.biz
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
2000
2000
1000
1000
0
6000
Check Qty
2000
2000
1000
1000
0
6000
NG Qty
5
8
0
0
0
13
 
Scrap 0
Rework 13
Under Deviation 0
Containment Action
100% VISUAL INSPECTION TO BE DONE
 
3. Process Flow
Process Flow Description
10 RECEIVING INSPECTION 20 STORAGE 30 BLANKING 40 1st BENDING ( `U` BENDING) 50 FINAL BENDING ( ROUNDING ) 60 MIG WELDING 70 FLAIRING 1st 80 FLAIRING 2nd 90 ID SIZING 100 SIDE GRINDING & BUFFING 110 BROACHING 120 HEAD GRINDING 130 OUTSIDE MOVEMENT FOR PLATING 140 STORAGE & RQC INSP. OF PLATED MATERIAL 150 FINAL INSPECTION 160 PACKING & DISPATCH
 
4. Process Details
Process / Operation WELDING
Outsource No
Machine / Cell MIG WELDING MACHINE
Machine / Cell No. MACHINE NO 6,7
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ToolNOZZELE TIP WAS NOT CLEANTIP CLEANIN G FREQUENCY WAS DEFINEDO
ManUNTRAINED OPERATOROPERATOR WAS UNDER TRIALX
MethodSYATEM WAS NOT DEFINED FOR HANDLING OF OPERATOR TRIAL PARTSPART FOUND NG DURING OPERATOR TRIALX
MaterialMIG WIRE DIA WAS UNDER SIZE/ OVER SIZEMIG WIRE DIA WAS OK AS PER DEFINEDO
MachineMACHINE WAS NOT OKMACHINE OKO
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method VISUAL
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size IS:2500
7. Root Cause Analysis (Occurance)
Why 1 WELDING CRACK IN PART
Why 2 WELDING MATERIAL NOT FILL COMPLETELY IN THE GAP
Why 3 OPERATOR WAS SEMISKILLED
Why 4 OPERATOR WAS UNDER TRIAL
Why 5
Root Cause (Occurance) 1-OPERATOR WAS UNDER TRIAL 2- SYSTEM WAS NOT DEFINED TO HANDLING THE OPERATOR TRIAL PARTS
 
Root Cause Analysis (Outflow)
Why 1 OK & NG PART MIXUP
Why 2 SYSTEM WAS NOT DEFINED TO HALDING THE OPERATOR TRIAL PARTS
Why 3
Why 4
Why 5
Root Cause (Outflow) SYSTEM WAS NOT DEFINED TO HALDING THE OPERATOR TRIAL PARTS
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
Outflow100% VISLA INSPECTION TE BE STARTEDNICE06/06/202306/06/2023Completed
OccuranceLOCATION TO BE DEFINED FOR OPERATOR TRIAL PARTSNICE06/06/202306/06/2023Completed
OccuranceOPERATOR OBSERVATION SYSTEM TO BE STARTED DURING TRIAL PERIODNICE06/06/202306/06/2023Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 100 % VISUAL INSPECTION
Inspection Method Other
Other Inspection Method OPL TO BE DISPLAYED
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) NO ANY WELDING AREA FOR UNDER TRIAL WELDER
463_Occurance_Before.jpg
Occurance (After) WELDING AREA MADE FOR UNDER TRIAL WELDER
463_Occurance_After.jpg
Outflow (Before) NO ANY SEPRATE AREA FOR OPERATOR TRIAL PARTS
463_Outflow_Before.jpg
Outflow (After) AREA MADE FOR OPERATOR TRIAL PARTS
463_Outflow_After.jpg
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant OTHER WELDING PART - BOTTOM ACK
 
12. Document Review
Documents WISOP
Specify Other Document WI & OPL
 
13. Effectiveness Of Action
Reviewed Quantity 500
Reason for submission