QFR No - 8000831919
Defect Details
NC No. 8000831919
NC Date 07/06/2023
NC Submission Date
Part No. F2DZ03912B
Part Name FORK BOLT-AABM
Supplier Name & Code 100539-N P ENTERPRISES
ETL Plant 1117-ETL K-228/9 Suspension
Defect Details NOT AS PER SPECIFICATION- IMPROPER BUFFING OBSERVED
 
1. Problem Description
Defect Description Buffing step mark on the top face of fork bolt (AABM)
Detection Stage Receipt
Problem Severity Aesthetic
NG Quantity 440
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID quality@npcindustries.in
Plant Head/CEO Email ID anand@npcindustries.in
MD Email ID ajay@npcindustries.in
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
1000
1200
0
0
0
2200
Check Qty
1000
1200
0
0
0
2200
NG Qty
440
300
0
0
0
740
 
Scrap 0
Rework 740
Under Deviation 0
Containment Action
Checked visually
 
3. Process Flow
Process Flow Description
10 - Raw Material 20 - Cutting and Forging(1st) 30-Forging(2nd) 40-Annealing 50-Phosphating 60 - Forging(3rd) I.D 70-Forging(4th) Hex 80 - CNC(1st) 90 - CNC(2nd) 100 - CNC(3rd) 110 - CNC drilling and Chamfering 120 - Final inspection 130 - Packing & Dispatch 140 - Buffing-1st 150 - Buffing 2nd 160 - Plating
 
4. Process Details
Process / Operation Buffing
Outsource Yes
Machine / Cell Buffing
Machine / Cell No. Buffing Machine
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ManUnskilled operator used for Buffing operationOperator observed to be skilledO
ManOperator unaware of defectOperator observed to be awareO
MaterialChemical composition not as per StdChemical composition observed as per StdO
ToolUse Wrong Size toolAfter verification we found operator was use wrong size of toolX
MethodRejected material mixedAfter verification we found Rejected material was not mix with ok partsO
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 Step mark observed on fork bolt.
Why 2 Excess material remove from the work pieces.
Why 3 Use High grain size ceramic belt use .
Why 4 Belt size did not define.
Why 5
Root Cause (Occurance) Ceramic Belt grain size did not define
 
Root Cause Analysis (Outflow)
Why 1 Could not be detected during Sampling inspection
Why 2 Sampling plan unable to catch defective part
Why 3 Sampling plan inadequate
Why 4 IS 2500 Sampling plan used
Why 5
Root Cause (Outflow) Sampling plan is not sufficient.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OutflowQ- alert to be displayed at buffing station & inspection station.Mr. Princ09/06/202308/06/2023Completed
Outflow100% inspection for Fork Bolt .Mr. Deepak04/07/202310/06/2023Completed
OccuranceChange Ceramic Belt grain size 80 and 120 to 220 and 620Mr. Gurpreet Singh28/06/202313/06/2023Completed
Occuranceuse of warn buffing wheel for better finishing.Mr. Gurpreet Singh28/06/202313/06/2023Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 100% Inspection should be done after buffing.
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection No
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) used of wrong size belt
466_Occurance_Before.png
Occurance (After) belt replace with wheel and currently using of warn buffing wheel.
466_Occurance_After.png
Outflow (Before) used of sampling inspection plan
466_Outflow_Before.jpg
Outflow (After) 100% inspection should be done after buffing
466_Outflow_After.png
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant Buffing Shop
 
12. Document Review
Documents ControlPlan, PFMEA, WISOP, ProcessFlowChart, InspCheckSheet
Specify Other Document no
 
13. Effectiveness Of Action
Reviewed Quantity 100
Reason for submission Verified and found ok