QFR No - 8000832050
Defect Details
NC No. 8000832050
NC Date 08/06/2023
NC Submission Date
Part No. F2BZ05712B
Part Name CAP OIL LOCK - J1D FF (10mm taper)
Supplier Name & Code 101255-MAHAVIR INDUSTRIES
ETL Plant 1117-ETL K-228/9 Suspension
Defect Details NOT AS PER SPECIFICATION-PARALLISUM FOUND NOT OK.
 
1. Problem Description
Defect Description RE-J1A Cap oil lock parallelism found not ok Observed 0.20 mm , required - 0.020 mm
Detection Stage Receipt
Problem Severity Fitment
NG Quantity 95
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID quality@mahavirind.co.in
Plant Head/CEO Email ID production@mahavirind.co.in
MD Email ID
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
300
0
0
0
0
300
Check Qty
300
0
0
0
0
300
NG Qty
95
0
0
0
0
95
 
Scrap 0
Rework 95
Under Deviation 0
Containment Action
All Suspected Material Verify at the Customer End.
 
3. Process Flow
Process Flow Description
RM Inward - Store- Parting-OD Grinding- CNC Turning - Plating - Final Inspection - Dispatch
 
4. Process Details
Process / Operation CNC TURNING
Outsource Yes
Machine / Cell CNC Section
Machine / Cell No. CNC-2/ CNC
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MachineParellity out after CNC machiningHeavy Burr Sticked with CNC JawO
 
6. Inspection Method Analysis (Current)
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 10pcs/Hr
7. Root Cause Analysis (Occurance)
Why 1 Pararellity Not OK
Why 2 During CNC machining job Out
Why 3 Heavy Burr Stick With CNC Jaw
Why 4 Not Air Flushing By Operator
Why 5
Root Cause (Occurance) 1)Heavy Burr Stick With CNC Jaw. 2)Not Air Flushing By Operator
 
Root Cause Analysis (Outflow)
Why 1 Pararellity Not OK
Why 2 Paralelity Over Than Required
Why 3 Not detected During Simple Step Gauge Inspection
Why 4 Variable Gauge Not Available For Correction
Why 5
Root Cause (Outflow) Variable Gauge Not Available For Correction
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceAir Flushing During Each and every part Feeding .Mr. Pralhad Bhawar24/06/202326/06/2023Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Plunger Dial Provide on Machine
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 20nos
10. Evidance of Countermeasure
Occurance (Before) Air Gun Facility not Available
467_Occurance_Before.jpeg
Occurance (After) 100% Air Gun Facility Provide On Machinie .
467_Occurance_After.jpeg
Outflow (Before) Step Gauge For Parellelity Inspection
467_Outflow_Before.jpeg
Outflow (After) Dial Gauge Provide On Machine .
467_Outflow_After.jpeg
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant For All Cap Oil Lock
 
12. Document Review
Documents ControlPlan, WISOP
Specify Other Document YES
 
13. Effectiveness Of Action
Reviewed Quantity
Reason for submission