QFR No - 8000832050
Defect Details
NC No. | 8000832050 |
NC Date | 08/06/2023 |
NC Submission Date | |
Part No. | F2BZ05712B |
Part Name | CAP OIL LOCK - J1D FF (10mm taper) |
Supplier Name & Code | 101255-MAHAVIR INDUSTRIES |
ETL Plant | 1117-ETL K-228/9 Suspension |
Defect Details | NOT AS PER SPECIFICATION-PARALLISUM FOUND NOT OK. |
1. Problem Description
Defect Description | RE-J1A Cap oil lock parallelism found not ok Observed 0.20 mm , required - 0.020 mm |
Detection Stage | Receipt |
Problem Severity | Fitment |
NG Quantity | 95 |
Is Defect Repeatative? | No |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | quality@mahavirind.co.in |
Plant Head/CEO Email ID | production@mahavirind.co.in |
MD Email ID |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
300
|
0
|
0
|
0
|
0
|
300
|
Check Qty |
300
|
0
|
0
|
0
|
0
|
300
|
NG Qty |
95
|
0
|
0
|
0
|
0
|
95
|
Scrap | 0 |
Rework | 95 |
Under Deviation | 0 |
Containment Action |
---|
All Suspected Material Verify at the Customer End. |
3. Process Flow
Process Flow Description |
---|
RM Inward - Store- Parting-OD Grinding- CNC Turning - Plating - Final Inspection - Dispatch |
4. Process Details
Process / Operation | CNC TURNING |
Outsource | Yes |
Machine / Cell | CNC Section |
Machine / Cell No. | CNC-2/ CNC |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Machine | Parellity out after CNC machining | Heavy Burr Sticked with CNC Jaw | O |
6. Inspection Method Analysis (Current)
Inspection Method | Instrument |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 10pcs/Hr |
7. Root Cause Analysis (Occurance)
Why 1 | Pararellity Not OK |
Why 2 | During CNC machining job Out |
Why 3 | Heavy Burr Stick With CNC Jaw |
Why 4 | Not Air Flushing By Operator |
Why 5 | |
Root Cause (Occurance) | 1)Heavy Burr Stick With CNC Jaw. 2)Not Air Flushing By Operator |
Root Cause Analysis (Outflow)
Why 1 | Pararellity Not OK |
Why 2 | Paralelity Over Than Required |
Why 3 | Not detected During Simple Step Gauge Inspection |
Why 4 | Variable Gauge Not Available For Correction |
Why 5 | |
Root Cause (Outflow) | Variable Gauge Not Available For Correction |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Air Flushing During Each and every part Feeding . | Mr. Pralhad Bhawar | 24/06/2023 | 26/06/2023 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | Plunger Dial Provide on Machine |
Inspection Method | Instrument |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 20nos |
10. Evidance of Countermeasure
Occurance (Before) |
Air Gun Facility not Available 467_Occurance_Before.jpeg |
Occurance (After) |
100% Air Gun Facility Provide On Machinie . 467_Occurance_After.jpeg |
Outflow (Before) |
Step Gauge For Parellelity Inspection 467_Outflow_Before.jpeg |
Outflow (After) |
Dial Gauge Provide On Machine . 467_Outflow_After.jpeg |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | For All Cap Oil Lock |
12. Document Review
Documents | ControlPlan, WISOP |
Specify Other Document | YES |
13. Effectiveness Of Action
Reviewed Quantity | |
Reason for submission |