QFR No - 8000832053
Defect Details
NC No. 8000832053
NC Date 08/06/2023
NC Submission Date
Part No. 520DZ00212
Part Name FORK BOLT K60-(DS181012)
Supplier Name & Code 101263-SINGLA PRECISION SCREWS
ETL Plant 1117-ETL K-228/9 Suspension
Defect Details NOT AS PER SPECIFICATION-INCOMPLETE THEADING OBSERVED
 
1. Problem Description
Defect Description M10 Threading operation incomplete
Detection Stage Receipt
Problem Severity Fitment
NG Quantity 10
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID quality@singlaprecision.com
Plant Head/CEO Email ID quality@singlaprecision.com
MD Email ID aditya@singlaprecision.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
2500
2000
0
1500
1000
7000
Check Qty
2500
2000
0
1500
1000
7000
NG Qty
1
0
0
0
0
1
 
Scrap 1
Rework 0
Under Deviation 0
Containment Action
We checked 100 % material lying at various stages.
 
3. Process Flow
Process Flow Description
1. RM INCOMING 2. CNC TURNING 3. TAPPING 4. THREAD ROLLING 5. PLATING 6. RE-TAPPING CHECK 7. FINAL INSPECTION 8. PACKING
 
4. Process Details
Process / Operation TAPPING
Outsource No
Machine / Cell TAPPING MACHINE
Machine / Cell No. TP02
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodINSPECTION PLAN NOT EFFECTIVEVALIDATED AND FOUND INSPECTION PLAN NOT EFFECTIVE SO PART SKIPPED FROM INSPECTIONX
MaterialRM GRADE AND SIZE NOT OKVALIDATED AND FOUND OKO
ManUNAWARENESS OF OPERATORVALIDATED AND FOUND OPERATOR WAS NEW AND PUT THE INCOMPLETE OPERATION PART IN FINISHED PARTSX
ToolTOOL MAY WEARVALIDATED AND FOUND OKO
MachineNUT BOLTS MAY LOOSENut of limit switch got loose due to which slide plate got tilted and tap not came to its position.O
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 5 PCS/HOUR
7. Root Cause Analysis (Occurance)
Why 1 M10 THREAD INCOMPLETE
Why 2 PROBLEM OCCURED AT TAPPING STAGE
Why 3 Nut of limit switch got loose due to which slide plate got tilted and tap not came to its position and threading operations left incomplete.
Why 4 THE OPERATOR WAS UNAWARE AND PUT THE INCOMPLETE OPERATION PART IN FINISHED PART BIN.
Why 5 SO NG PART MIXED WITH FINISHED PARTS
Root Cause (Occurance) Nut of limit switch got loose due to which slide plate got tilted and tap not came to its position and threading operations left incomplete.THE OPERATOR WAS UNAWARE AND PUT THE INCOMPLETE OPERATION PART IN FINISHED PART BIN.SO NG PART MIXED WITH FINISHED PARTS.
 
Root Cause Analysis (Outflow)
Why 1 M10 THREAD INCOMPLETE
Why 2 INSPECTION PLAN WAS NOT EFFECTIVE
Why 3 NG PART SKIPPED FROM INSPECTION
Why 4 SO NG PART DELIEVERED TO CUSTOMER
Why 5
Root Cause (Outflow) INSPECTION PLAN WAS NOT EFFECTIVE.NG PART SKIPPED FROM INSPECTION.SO NG PART DELIEVERED TO CUSTOMER.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OutflowINSPECTION FREQUENCY CHANGED TO 100%GANESH MAURYA12/06/202312/06/2023Completed
OccuranceDouble nut lock tightening done to prevent the nut from loosing and Training given to Operator regarding putting the NG part into Red bin.Ganesh Maurya12/06/202312/06/2023Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 100% RETAPPING CHECK DONE AFTER PLATING PROCESS.
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 50/1200
10. Evidance of Countermeasure
Occurance (Before) Nut of limit was loose.
469_Occurance_Before.pdf
Occurance (After) Double nut lock tightening done to prevent it from loosing.
469_Occurance_After.pdf
Outflow (Before) INSPECTION FREQUENCY WAS 5 PCS/HOUR
469_Outflow_Before.pdf
Outflow (After) INSPECTION FREQUENCY UPDATED
469_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant FORK BOLT PRFH,FORK BOLT BOXER,FORK BOLT HMS-30
 
12. Document Review
Documents ControlPlan, WISOP
Specify Other Document NO
 
13. Effectiveness Of Action
Reviewed Quantity 100
Reason for submission Verified next 3 lot and found