QFR No - 8000832689
Defect Details
NC No. | 8000832689 |
NC Date | 12/06/2023 |
NC Submission Date | |
Part No. | 16JPP00117 |
Part Name | WHEEL CLUTCH REML 6 PLATE / 7 PLATE |
Supplier Name & Code | 101100-CAST 4 ALUMINIUM PVT LTD |
ETL Plant | 1132-ETL K-226/1 TRANSMISSION |
Defect Details | RUN OUT MORE-TEETH ID R/O OBS 1.0 MM |
1. Problem Description
Defect Description | Tapper Machining -Teeth Runout found more than 1 mm against 0.2 |
Detection Stage | Inprocess |
Problem Severity | Fitment |
NG Quantity | 159 |
Is Defect Repeatative? | No |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | info@cast4aluminium.com |
Plant Head/CEO Email ID | infor@cast4aluminium.com |
MD Email ID | kiran@cast4aluminium.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
500
|
0
|
0
|
200
|
1300
|
2000
|
Check Qty |
500
|
0
|
0
|
200
|
1300
|
2000
|
NG Qty |
159
|
0
|
0
|
200
|
1300
|
1659
|
Scrap | 1659 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
Pipeline Material checked 100 % for defects & Material quarantined and Scrapped. |
3. Process Flow
Process Flow Description |
---|
RM- Melting- PDC - Gate cutting / Fettling- Machining - Final inspection - FG- PDI - Dispatch |
4. Process Details
Process / Operation | Machining |
Outsource | No |
Machine / Cell | CNC machining |
Machine / Cell No. | CNC Machining |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Machine | Jaw observed cracked. | Jaw observed cracked. | O |
Man | Part skipped from inspection As inspector is not aware of defect. | Part skipped from inspection As inspector is not aware of defect. | O |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | Visual |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
7. Root Cause Analysis (Occurance)
Why 1 | REML 6 plate wheel observed with taper machining |
Why 2 | During Machining operation job get shifted from location. |
Why 3 | Job is not get clamped properly in jaw. |
Why 4 | Jaw observed cracked |
Why 5 | |
Root Cause (Occurance) | Jaw observed cracked |
Root Cause Analysis (Outflow)
Why 1 | Jaw observed cracked |
Why 2 | Inspector is not aware of defect |
Why 3 | |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | Inspector is not aware of defect |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Jaw observed cracked | Datta | 10/06/2023 | Completed | |
Outflow | Detection poka-yoke provided at drilling &Tapping stage ( Part located in ID & Three spline hole ). OPL is displayed 3) Knowledge & training is provided to inspectors. | Manoj C | 10/06/2023 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | No |
Change Details | No change , OPL is displayed & training provided to inspectors |
Inspection Method | Other |
Other Inspection Method | VIsual |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
Jaw observed Crack 472_Occurance_Before.xlsx |
Occurance (After) |
Replaced with New 472_Occurance_After.xlsx |
Outflow (Before) |
Visual 472_Outflow_Before.xlsx |
Outflow (After) |
Visual with Training provided to Inspector & OPL is displayed 472_Outflow_After.xlsx |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | Applied to other Machines & Components ( wheels) |
12. Document Review
Documents | WISOP |
Specify Other Document | OPL |
13. Effectiveness Of Action
Reviewed Quantity | 1000 |
Reason for submission | Ok |