QFR No - 8000833697
Defect Details
NC No. 8000833697
NC Date 21/06/2023
NC Submission Date
Part No. 520FZ01902
Part Name HUB CLUTCH K70
Supplier Name & Code 100656-MADHURA DIE CAST PVT.LTD
ETL Plant 1132-ETL K-226/1 TRANSMISSION
Defect Details EXCESS M/CING-DIMN 21.20-0.25 OBS 20.73~2095 MM
 
1. Problem Description
Defect Description Tapper Machining Dimn 21.20-0.25 mm found up to 20.73~20.95 mm
Detection Stage Inprocess
Problem Severity Function
NG Quantity 2
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID madhuradiecast@gmail.com
Plant Head/CEO Email ID madhuradiecast@gmail.com
MD Email ID madhuradiecast@gaikegroup.in
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
1500
0
0
1000
1500
4000
Check Qty
1500
0
0
1000
1500
4000
NG Qty
2
0
0
0
0
2
 
Scrap 2
Rework 0
Under Deviation 0
Containment Action
100% Stock Segregation done at the Customer end, supplier end with blue dot marking
 
3. Process Flow
Process Flow Description
1.Casting 2.fetling 3. CNC 1st Set-up 4.CNC 2nd Set-up 5.Broaching 6.Final Inspection
 
4. Process Details
Process / Operation CNC 1st Set-up
Outsource No
Machine / Cell CNC
Machine / Cell No. CNC N0.01
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodComponent was not clamp properResting area of component was checkedX
ManTraining not given to operatorTraining plan and on job training record checkedO
ManAttitude of Operator is not good against workInterview with operator found okO
MaterialDamage on Component Resting areaTrial taken for damage component found NGX
MachineJaw Clamping pressure was lowJaw clamping pressure found okO
ManLow skill level operator on MachineSkill matrix chart verify found okO
ToolJaw runout is not okSet-up approval report checked found as per control planO
ToolBurr on Component resting area in jawAir gun available on CNC machining stageO
 
6. Inspection Method Analysis (Current)
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection No
Checking Freq. Sampling
Sampling No
Sample Size 05
7. Root Cause Analysis (Occurance)
Why 1 Tapper Machining Dim 21.20-0.25 mm found up to 20.73~20.95 mm
Why 2 Component was not clamp proper
Why 3 Damage on Component Resting area
Why 4
Why 5
Root Cause (Occurance) Damage on Component Resting area
 
Root Cause Analysis (Outflow)
Why 1 Inspection Eye sequence chart not updated at fettling stage
Why 2 This defect not added
Why 3
Why 4
Why 5
Root Cause (Outflow) Inspection Eye sequence chart not updated at fettling stage
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
Occurance1. Rubber mat provided in casting stage. 2.Work instruction is updated for fettling operation damage defect checking and kept on red bin.Production Supervisor19/06/202321/06/2023Completed
Outflow1.QA Alert displayed on Final stage 2.OPL displayed Casting,Fettling & Machining stage 3.Training given to Operator & Final Inspector.QA Engineer20/06/202321/06/2023Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System No
Change Details NO
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 1:25
10. Evidance of Countermeasure
Occurance (Before) Work Instruction not updated for fettling operation
488_Occurance_Before.jpg
Occurance (After) 1. Rubber mat provided in casting stage. 2.Work instruction is updated for fettling operation damage defect checking and kept on red bin.
488_Occurance_After.pdf
Outflow (Before) Training and awareness not given to inspector and operator about defect
488_Outflow_Before.jpeg
Outflow (After) 1.QA Alert displayed on Final stage 2.OPL displayed Casting,Fettling & Machining stage 3.Training given to Operator & Final Inspector.
488_Outflow_After.jpeg
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant no
 
12. Document Review
Documents WISOP, InspCheckSheet
Specify Other Document OPL
 
13. Effectiveness Of Action
Reviewed Quantity 1000
Reason for submission OK