QFR No - 8000833697
Defect Details
NC No. | 8000833697 |
NC Date | 21/06/2023 |
NC Submission Date | |
Part No. | 520FZ01902 |
Part Name | HUB CLUTCH K70 |
Supplier Name & Code | 100656-MADHURA DIE CAST PVT.LTD |
ETL Plant | 1132-ETL K-226/1 TRANSMISSION |
Defect Details | EXCESS M/CING-DIMN 21.20-0.25 OBS 20.73~2095 MM |
1. Problem Description
Defect Description | Tapper Machining Dimn 21.20-0.25 mm found up to 20.73~20.95 mm |
Detection Stage | Inprocess |
Problem Severity | Function |
NG Quantity | 2 |
Is Defect Repeatative? | No |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | madhuradiecast@gmail.com |
Plant Head/CEO Email ID | madhuradiecast@gmail.com |
MD Email ID | madhuradiecast@gaikegroup.in |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
1500
|
0
|
0
|
1000
|
1500
|
4000
|
Check Qty |
1500
|
0
|
0
|
1000
|
1500
|
4000
|
NG Qty |
2
|
0
|
0
|
0
|
0
|
2
|
Scrap | 2 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
100% Stock Segregation done at the Customer end, supplier end with blue dot marking |
3. Process Flow
Process Flow Description |
---|
1.Casting 2.fetling 3. CNC 1st Set-up 4.CNC 2nd Set-up 5.Broaching 6.Final Inspection |
4. Process Details
Process / Operation | CNC 1st Set-up |
Outsource | No |
Machine / Cell | CNC |
Machine / Cell No. | CNC N0.01 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Method | Component was not clamp proper | Resting area of component was checked | X |
Man | Training not given to operator | Training plan and on job training record checked | O |
Man | Attitude of Operator is not good against work | Interview with operator found ok | O |
Material | Damage on Component Resting area | Trial taken for damage component found NG | X |
Machine | Jaw Clamping pressure was low | Jaw clamping pressure found ok | O |
Man | Low skill level operator on Machine | Skill matrix chart verify found ok | O |
Tool | Jaw runout is not ok | Set-up approval report checked found as per control plan | O |
Tool | Burr on Component resting area in jaw | Air gun available on CNC machining stage | O |
6. Inspection Method Analysis (Current)
Inspection Method | Instrument |
Other Inspection Method | |
Check Point at Final Inspection | No |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 05 |
7. Root Cause Analysis (Occurance)
Why 1 | Tapper Machining Dim 21.20-0.25 mm found up to 20.73~20.95 mm |
Why 2 | Component was not clamp proper |
Why 3 | Damage on Component Resting area |
Why 4 | |
Why 5 | |
Root Cause (Occurance) | Damage on Component Resting area |
Root Cause Analysis (Outflow)
Why 1 | Inspection Eye sequence chart not updated at fettling stage |
Why 2 | This defect not added |
Why 3 | |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | Inspection Eye sequence chart not updated at fettling stage |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | 1. Rubber mat provided in casting stage. 2.Work instruction is updated for fettling operation damage defect checking and kept on red bin. | Production Supervisor | 19/06/2023 | 21/06/2023 | Completed |
Outflow | 1.QA Alert displayed on Final stage 2.OPL displayed Casting,Fettling & Machining stage 3.Training given to Operator & Final Inspector. | QA Engineer | 20/06/2023 | 21/06/2023 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | No |
Change Details | NO |
Inspection Method | Instrument |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 1:25 |
10. Evidance of Countermeasure
Occurance (Before) |
Work Instruction not updated for fettling operation 488_Occurance_Before.jpg |
Occurance (After) |
1. Rubber mat provided in casting stage. 2.Work instruction is updated for fettling operation damage defect checking and kept on red bin. 488_Occurance_After.pdf |
Outflow (Before) |
Training and awareness not given to inspector and operator about defect 488_Outflow_Before.jpeg |
Outflow (After) |
1.QA Alert displayed on Final stage 2.OPL displayed Casting,Fettling & Machining stage 3.Training given to Operator & Final Inspector. 488_Outflow_After.jpeg |
11. Horizontal Deployment
Horizontal Deployment Required | No |
Applicable Machine / Model / Plant | no |
12. Document Review
Documents | WISOP, InspCheckSheet |
Specify Other Document | OPL |
13. Effectiveness Of Action
Reviewed Quantity | 1000 |
Reason for submission | OK |