QFR No - 8000834573
Defect Details
NC No. 8000834573
NC Date 26/06/2023
NC Submission Date
Part No. 538LT00112
Part Name SILENT BLOCK PLATED
Supplier Name & Code 101023-FORES ELASTOMECH INDIA PVT. LT
ETL Plant 1118-ETL E-92,93 Suspension
Defect Details DAMAGES-SHORTMOLDING:4NO,CHAMFERO/D DAMAGE:275NO
 
1. Problem Description
Defect Description SHORT MOLDING & CHAMFER O/D DAMAGE
Detection Stage Inprocess
Problem Severity Aesthetic
NG Quantity 279
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID malani.pritam@foresgroup.com
Plant Head/CEO Email ID singh.barinder@foresgroup.com
MD Email ID swamy.pj@foresgroup.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
28000
0
0
35000
0
63000
Check Qty
28000
0
0
35000
0
63000
NG Qty
279
0
0
10
0
289
 
Scrap 289
Rework 0
Under Deviation 0
Containment Action
100 % Sorting done at customer end at ETL With special marking . 100 % Sorting done at M/s Fore End with Special identification on Box .
 
3. Process Flow
Process Flow Description
Receiving the material - (Inspect the Raw material , Inspect the insert, Inspect the Outer - Compound Batch - Moulding - Deflashing -Plating - Visual inspection - ID & Height inspection - Bond testing - Packaging -Dispatch.
 
4. Process Details
Process / Operation Moulding
Outsource No
Machine / Cell Moulding
Machine / Cell No. INJ-250T
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MaterialWrong material usedverified the last six month data of hardness & Found okayO
MachineWeak joint of in metal to rubber.NG part verify & Found not okay .X
ToolTool not as per requirement .Verified the tool as per PM inspection sheet & Found okay .O
ManSkipped from inspectionInspection method not okayX
MethodInsert & Outer loading method not oakyverified the loading fixture & Found okayO
MachineLess or more temperatureverified the data for temperature & found okay .O
MachineLess or more cure timeverify the parameter & found okay .O
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 Short Moulding
Why 2 less material flow in mould cavity tool
Why 3 material gate flow point broken by previous shot gate .
Why 4 Gate is being broken from both end due to design constraint.
Why 5
Root Cause (Occurance) Gate is being broken from both end due to design constraint.
 
Root Cause Analysis (Outflow)
Why 1 Skipped form inspection.
Why 2 defect not detect in inspection stage .
Why 3 difficult to inspect this defect.
Why 4 inspection method not okay.
Why 5
Root Cause (Outflow) inspection method not okay.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceGate point will check in every shot on rubber pad or part.Mr Zukle26/06/202326/06/2023Completed
OutflowVisual inspection will start on magnified glass With white background on table .Mr motilal .26/06/202322/06/2023Completed
OccuranceTraining given to operator .Mr Zukle26/06/202326/06/2023Completed
OutflowAwareness & training given to inspectorMr motilal26/06/202326/06/2023Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System No
Change Details N/A
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) 1.Gate is being broken from both end due to design constraint.
497_Occurance_Before.docx
Occurance (After) 1.Gate point will check in every shot on rubber pad or part. 2.Training given to operator. 3.opl display at operation stage.
497_Occurance_After.pdf
Outflow (Before) inspection method not okay.
497_Outflow_Before.pptx
Outflow (After) 1.Visual inspection will start on magnified glass With white background on table . 2.Opl display at inspection stage . 3.training & awareness given to inspector
497_Outflow_After.jpg
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant Applicable for all part
 
12. Document Review
Documents WISOP
Specify Other Document N/A
 
13. Effectiveness Of Action
Reviewed Quantity
Reason for submission