QFR No - 8000834704
Defect Details
NC No. 8000834704
NC Date 27/06/2023
NC Submission Date
Part No. 550FA17433
Part Name FORK PIPE MACHINED
Supplier Name & Code 100503-DIVYA INDUSTRIES
ETL Plant 1116-ETL K-120 Suspension
Defect Details NOT AS PER SPECIFICATION-CLUCKING,THREADING,LENGTH NOT OK
 
1. Problem Description
Defect Description Dimensional NG concern observed.
Detection Stage Receipt
Problem Severity Fitment
NG Quantity 148
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID quality@mahavirind.co.in
Plant Head/CEO Email ID planthead@mahavirind.co.in
MD Email ID rajesh@mahavirind.co.in
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
1600
0
0
0
0
1600
Check Qty
1600
0
0
0
0
1600
NG Qty
148
0
0
0
0
148
 
Scrap 0
Rework 148
Under Deviation 0
Containment Action
All Suspected material Checking At Customer End
 
3. Process Flow
Process Flow Description
Raw material Inward- Store- CNC Machining Coulking Side- CNC Machining Threading Side - 1.5 mm Cross Drill - Final Inspection - Packing - Rusty Oil Apply - Dispatch - Transport .
 
4. Process Details
Process / Operation CNC Machining - Coulking Side.
Outsource No
Machine / Cell CNC No.2
Machine / Cell No. Fork Pipe CNC Sect.
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MachineCoulking Under Size Coolant Flow Not properCoolant Pipe Accessory Not Available On MachineO
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 Coulking Side ID under size
Why 2 Insert Wear
Why 3 Not Proper Coolant Flow
Why 4 Not proper Coolant Pipe Arrangement .
Why 5
Root Cause (Occurance) Not proper Coolant Pipe Arrangement.
 
Root Cause Analysis (Outflow)
Why 1 Coulking Side ID under size
Why 2 during final inspection defected part not detect
Why 3 Randombly Defect
Why 4
Why 5
Root Cause (Outflow) During final inspection defected part not detect.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceAll Machine Coolant Pipe Replace And Flexible Pipe provideMantenanace Head and production Head05/07/202308/07/2023Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 100% ID Inspection
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Not proper Coolant Pipe Arrangemen
499_Occurance_Before.docx
Occurance (After) All Machine Coolant Pipe Replace And Flexible Pipe provide
499_Occurance_After.docx
Outflow (Before) 1) Go Gauge Not Proper suit in ID .2)Coulking ID Inspection Frequency was 5Nos / Hr.
499_Outflow_Before.docx
Outflow (After) 1) Go gauge Proper Suit Coulking ID .2)Inspection Frequency Change Now 20nos/hr
499_Outflow_After.docx
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant All Fork Pipe Coolant Pipe Replace
 
12. Document Review
Documents ControlPlan, PFMEA
Specify Other Document No
 
13. Effectiveness Of Action
Reviewed Quantity 10
Reason for submission Corrective action parts submission.