QFR No - 8000834724
Defect Details
NC No. | 8000834724 |
NC Date | 27/06/2023 |
NC Submission Date | |
Part No. | S2AB02207B |
Part Name | ADJUSTER POWDER COATED KTEM |
Supplier Name & Code | 100973-TESMO MOTORCAST PRIVATE LIMITE |
ETL Plant | 1116-ETL K-120 Suspension |
Defect Details | EXCESS MATERIAL-EXCESS MATERIAL AT SPRING RESTING FACE |
1. Problem Description
Defect Description | Excess material observed at spring resting face. |
Detection Stage | Receipt |
Problem Severity | Fitment |
NG Quantity | 19 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | rkhare@tesmomotorcast.com |
Plant Head/CEO Email ID | harish.bala@tesmomotorcast.com |
MD Email ID | svkallani@tesmomotorcast.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
2000
|
0
|
0
|
3000
|
10000
|
15000
|
Check Qty |
2000
|
0
|
0
|
3000
|
5000
|
10000
|
NG Qty |
20
|
0
|
0
|
2
|
300
|
322
|
Scrap | 20 |
Rework | 302 |
Under Deviation | 0 |
Containment Action |
---|
1). Pin flash rework process started. 2). 100% inspection before powder coating. |
3. Process Flow
Process Flow Description |
---|
C-REAMER-GRINDING-SURFACE TREATMENT-INSPECTION-POWDER COATING-SAMPLE INSPECTION-PACKING DESPATCH |
4. Process Details
Process / Operation | PDC |
Outsource | No |
Machine / Cell | HPDC MACHINE |
Machine / Cell No. | 350-1 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Material | INSERT MATERIAL NOT GOOD | CHEMICAL COMPOSITION VARIFICATION | O |
Machine | EJECITON NOT BALANCE | VISUAL CHECK FOR EJECTION PARALLILITY | O |
Tool | EJECTOR PIN DIA ON MOVING INSERT INCREASES | VERNIER | O |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | VISUAL |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 1 |
7. Root Cause Analysis (Occurance)
Why 1 | PIN FLASH ON SPRING RESTING FACE |
Why 2 | EJECTOR PIN INCREASE ON INSERT |
Why 3 | DIE RUNNING WITH UNBALANCE EJECTION |
Why 4 | SETTING NOT DONE CORRECTLY |
Why 5 | POOR SKILL LEVEL |
Root Cause (Occurance) | EJECTOR SETTING SKILL LEVEL NOT GOOD |
Root Cause Analysis (Outflow)
Why 1 | PIN FLASH ON SPRING RESTING FACE |
Why 2 | PIN FLASH CHECKING IS MISSED BY INSPECTOR |
Why 3 | IMPROPER TRAINING TO INSPECTOR |
Why 4 | VISUAL DISPLAY NOT AVAILABLE |
Why 5 | |
Root Cause (Outflow) | VISUAL DISPLAY OF PIN FLASH NOT AVAILABLE |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Outflow | PIN & DIAMETER CHECKING | SACHIN | 15/07/2023 | 15/07/2023 | Completed |
Occurance | VISUAL DISPLAY AT INSPECTION WITH PROPER TRAINING | RAHUL KHARE | 15/07/2023 | 15/07/2023 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | VISUAL DISPLAY IN INSPECTION TABLE WITH SAMPLE |
Inspection Method | Other |
Other Inspection Method | VISUAL |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 1 |
10. Evidance of Countermeasure
Occurance (Before) |
PART WITH PIN FLASH 500_Occurance_Before.jpg |
Occurance (After) |
EJECTOR PIN DIA INCREASE 500_Occurance_After.jpg |
Outflow (Before) |
PART WITH PIN FLASH 500_Outflow_Before.jpg |
Outflow (After) |
SAMPLE PLACED ON FINAL STAGE 500_Outflow_After.jpg |
11. Horizontal Deployment
Horizontal Deployment Required | No |
Applicable Machine / Model / Plant | NO |
12. Document Review
Documents | InspCheckSheet |
Specify Other Document | PART DISPLAY |
13. Effectiveness Of Action
Reviewed Quantity | 10 |
Reason for submission | Against reported defect. |