QFR No - 8000835012
Defect Details
NC No. 8000835012
NC Date 30/06/2023
NC Submission Date
Part No. C2PP00320B
Part Name WHEEL CLUTCH_C20009_D1
Supplier Name & Code 100432-BHAKTI AUTO COMP PRIVATE LIMIT
ETL Plant 1132-ETL K-226/1 TRANSMISSION
Defect Details TAPPING O/SIZE.-THREADING OVERSIZE ISSUE(PPG NOGO QUALIF
 
1. Problem Description
Defect Description Threading Oversize -Fitment bolt loose (Minor Diameter found oversize)
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 32
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID bhaktiauto2008@gmail.com
Plant Head/CEO Email ID bhaktiauto2008@gmail.com
MD Email ID vinodanin@gmail.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
400
0
0
400
800
1600
Check Qty
400
0
0
400
800
1600
NG Qty
32
0
0
0
0
32
 
Scrap 32
Rework 0
Under Deviation 0
Containment Action
100% lot verified at customer end Inhouse WIP & FG stock verified
 
3. Process Flow
Process Flow Description
Raw Material - Melting - Casting - Fettling - Face machining -6 hole Drill & Tapping - Inspection - PDI - Dispatch
 
4. Process Details
Process / Operation Drilling & Tapping
Outsource Yes
Machine / Cell machining
Machine / Cell No. 01
5. Problem Analysis
Type Possible Cause Fact Verification Jud
Manpart loading on fixturepart loose after clamingO
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 05
7. Root Cause Analysis (Occurance)
Why 1 Part No load properly on fixture
Why 2 Operator not able to judge the perfect loading of part on fixture
Why 3 Entry Level L1 Operator
Why 4
Why 5
Root Cause (Occurance) Part uneven clamping on fixture by semi skilled operator, Drilling hole shifted from its original lug position hence cause Minor ID Oversized
 
Root Cause Analysis (Outflow)
Why 1 at final inspection stage inspector not able to detect the oversized issue
Why 2 No check point for Minor ID inspection
Why 3
Why 4
Why 5
Root Cause (Outflow) Check point is not available hence not able to block defect in inspection
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceSkilled Manpower L3 allotted to D/T Operation.GS engineering08/07/202307/07/2023Completed
OutflowInspection check point addedBhakti Auto07/07/202307/07/2023Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details M6x1 Minor ID inspection check point is added in check sheet
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Semi Skilled operator
502_Occurance_Before.bmp
Occurance (After) skilled operator Provided
502_Occurance_After.bmp
Outflow (Before) No Check Point
502_Outflow_Before.jpg
Outflow (After) Check Point added in Inspection
502_Outflow_After.jpg
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant NA
 
12. Document Review
Documents ControlPlan
Specify Other Document Control plan
 
13. Effectiveness Of Action
Reviewed Quantity 1000
Reason for submission No repetition of Defect phenomenon