QFR No - 8000836624
Defect Details
NC No. 8000836624
NC Date 13/07/2023
NC Submission Date
Part No. 550FA18433
Part Name FORK PIPE MACHINED - K11
Supplier Name & Code 101222-SANGKAJ ENGINEERING PVT LTD- U
ETL Plant 1117-ETL K-228/9 Suspension
Defect Details NOT AS PER SPECIFICATION-QM-VL-KDH - THREADING NG
 
1. Problem Description
Defect Description Threading NG found at incoming
Detection Stage Receipt
Problem Severity Fitment
NG Quantity 108
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID irfan@sangkaj.com
Plant Head/CEO Email ID steel@sangkaj.com
MD Email ID anirudh.2007@hotmail.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
1000
0
0
0
0
1000
Check Qty
1000
0
0
0
0
1000
NG Qty
108
0
0
0
0
108
 
Scrap 108
Rework 0
Under Deviation 0
Containment Action
Segregation of all pipe line material at customer as well as warehouse and SEPL end.
 
3. Process Flow
Process Flow Description
10. RM Inward inspection 20.Identification groove 30.Induction hardening 40.Bend removal 50.CNC Turning First 60. CNC turning second 70. Drilling 80.Air Cleaning 90.Packing and Dispatch
 
4. Process Details
Process / Operation 50. CNC Turning First
Outsource No
Machine / Cell CNC Fork Pipe Cell
Machine / Cell No. Cell no.3
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodGauge Wear outGauge Wear outO
ToolTool wear outInsert/tool manufacturer changedO
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection No
Checking Freq. Sampling
Sampling No
Sample Size 5 per hour
7. Root Cause Analysis (Occurance)
Why 1 Thread undersize (Go not pass)
Why 2 Tool wear out before its life
Why 3 Wrong grade insert taken for use
Why 4 Insert grade/Manufacturer not mentioned in control plan.
Why 5
Root Cause (Occurance) Due Insert grade/Manufacturer not mentioned in control plan wrong grade insert taken for use.
 
Root Cause Analysis (Outflow)
Why 1 Thread undersize (Go not pass) not detected
Why 2 Part found ok on gauge
Why 3 Gauge wear out not detected
Why 4 Wear ring gauge not available
Why 5
Root Cause (Outflow) Wear ring gauge not available
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceAdd insert grade and Manufacturer in Control planMr. Krushna Fuke02/08/202301/08/2023Completed
OutflowProcure wear ring gaugeMr.Irfan30/08/202308/09/2023Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System No
Change Details Wear ring added
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection No
Checking Freq. Sampling
Sampling No
Sample Size Plan
10. Evidance of Countermeasure
Occurance (Before) Threading insert specification and Make not available
509_Occurance_Before.pdf
Occurance (After) Threading insert make and grade updated in control plan
509_Occurance_After.pdf
Outflow (Before) Wear gauge not available
509_Outflow_Before.xlsx
Outflow (After) wear gauge ordered and made available up to 30.08.23
509_Outflow_After.jpeg
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant All fork pipe model
 
12. Document Review
Documents ControlPlan, WISOP
Specify Other Document No
 
13. Effectiveness Of Action
Reviewed Quantity 150
Reason for submission Ok