QFR No - 8000839662
Defect Details
NC No. 8000839662
NC Date 07/08/2023
NC Submission Date
Part No. S1HT05507B
Part Name OUTER SPRING - K1JF
Supplier Name & Code 101225-HELICAL SPRINGS
ETL Plant 1146-ETL Suspension Narasapura
Defect Details DIMETER UNDERSIZE-ID LESS ISSUE
 
1. Problem Description
Defect Description K1JF Outer spring ID less issue
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 2
Is Defect Repeatative? No
Defect Sketch / Photo vegwl3chpj0cbxq1xrhmexwa.jpg
Supplier Communication Details
Quality Head Email ID shaikhmoin@helicalsprings.in
Plant Head/CEO Email ID shaikhmoin@helicalsprings.in
MD Email ID ataneja@helicalsprings.in
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
2000
0
0
1200
1000
4200
Check Qty
2000
0
0
1200
1000
4200
NG Qty
2
0
0
0
0
2
 
Scrap 2
Rework 0
Under Deviation 0
Containment Action
We Have Checked All At M/s Helical End Material Found OK.
 
3. Process Flow
Process Flow Description
Coiling>Stress-relieving-1>End Grinding>Shot-peening>Scragging>100% E1, E2 & Length Checking>ID Checking>Stress-Relieving-2>Powder Coating>Final Inspection>Packing>Dispatch.
 
4. Process Details
Process / Operation 100% ID Checking
Outsource No
Machine / Cell Plain Plug Gauge
Machine / Cell No. -
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodSetup spring not specific location.Location to be defined for setup spring.X
ManUnskilled OperatorSkill matrix checked found okO
MachineMachine check Sheet not followedCLIT verified found okO
MaterialMaterial GradeRMTC verified found okO
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 Inner Diameter Under Size
Why 2 RM Coil Change Initial Parts Mix-up
Why 3 No Location Defined for Coil Change Initial Parts
Why 4
Why 5
Root Cause (Occurance) RM Coil Change Initial Parts Mix-up
 
Root Cause Analysis (Outflow)
Why 1 Inner Diameter Undersize ( mix Up)
Why 2 ID Checked in Sampling Basis
Why 3 Due to less qty. not able to detect.
Why 4
Why 5
Root Cause (Outflow) RM Coil Change Initial Parts Mix-up
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
Outflow1.100% Inspection Started. 2. Training Provided to the Operators, Final Inspectors & RecordedQA20/08/2023Completed
OccuranceProcedure is Defined for Coil Change Parts HandlingQA & Production20/11/2023Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 100% ID Check Point Added.
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) WI And SOP Not Displayed for Coil Change Initial Parts Handling
516_Occurance_Before.pdf
Occurance (After) WI And SOP Displayed for Coil Change Initial Parts Handling
516_Occurance_After.pdf
Outflow (Before) Operator not aware.
516_Outflow_Before.pdf
Outflow (After) Training Given.
516_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant Horizontal Deployment Done For KOPG.
 
12. Document Review
Documents WISOP, InspCheckSheet
Specify Other Document Training Record
 
13. Effectiveness Of Action
Reviewed Quantity 1000
Reason for submission Reviewed 1000 found ok