QFR No - 8000839779
Defect Details
NC No. | 8000839779 |
NC Date | 08/08/2023 |
NC Submission Date | |
Part No. | B2EH08502O |
Part Name | END CONNECTOR MASTER SIDE NTORQ |
Supplier Name & Code | 101221-SUNREN AUTOMOTIVE PRIVATE LIMI |
ETL Plant | 1120-ETL K-226/2 Disc Brakes |
Defect Details | OTHER-LUG NOT OK |
1. Problem Description
Defect Description | LUG NOT OK |
Detection Stage | Receipt |
Problem Severity | Fitment |
NG Quantity | 1359 |
Is Defect Repeatative? | No |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | shivank@sunren.in |
Plant Head/CEO Email ID | dharmbir@sunren.in |
MD Email ID | subhashsaini@sunren.in |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
0
|
17000
|
9000
|
2000
|
3000
|
31000
|
Check Qty |
0
|
17000
|
9000
|
2000
|
3000
|
31000
|
NG Qty |
0
|
243
|
0
|
0
|
0
|
243
|
Scrap | 243 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
100% inspection will be carried out at warehouse and green dot marking is placed over the lug for ensurity. |
3. Process Flow
Process Flow Description |
---|
Inspection of Raw Material - Cutting Multi Operation - Centerless Grinding - Milling - Cross Drill - Neck Drill-Cross Reamer - Pin Drill - Pin Assembly - Brazing - Facing1st - Facing-2nd -Chamfer- 100% Visual Inspection -Bending - Plating - Final Inspection - Packaging - Storage / Dispatch . |
4. Process Details
Process / Operation | Bending |
Outsource | No |
Machine / Cell | Bending Fixture |
Machine / Cell No. | 10 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Man | Lack of Knowledge | Skill Matrix | O |
Method | Inspection Method Not Effective | Gauge Verification | X |
Tool | wear and tear of fixtures | Fixture Validation | X |
6. Inspection Method Analysis (Current)
Inspection Method | Sp. Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 5 |
7. Root Cause Analysis (Occurance)
Why 1 | wear & tear of bending fixture |
Why 2 | Fixture was not hardened |
Why 3 | Fixture life was not decided |
Why 4 | Fixture not validated |
Why 5 | Lack of awareness |
Root Cause (Occurance) | Wear & Tear of bending fixture |
Root Cause Analysis (Outflow)
Why 1 | Inspection process not effective |
Why 2 | Checking Gauge found not effective |
Why 3 | complete profile of the part was not covered in gauge |
Why 4 | Gauge Design Needs improvement |
Why 5 | Gauge Design not validated |
Root Cause (Outflow) | Checking Gauge Found Not Effective. |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Fixture will be replaced , Hardened , Gauge validation will be done and improvement will be done in bending fixture taking pin as a reference for bending. | Shivank | 29/09/2023 | 10/09/2023 | Completed |
Outflow | Checking gauge will be re-designed considering pin shifting , part profile and pin angle. | Shivank | 29/09/2023 | 27/09/2023 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | Lug shift is checked 200% and green dot marking is started over the lug for ensurity. |
Inspection Method | Sp. Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 5 |
10. Evidance of Countermeasure
Occurance (Before) |
Fixture Gets Wear and Tear. 518_Occurance_Before.png |
Occurance (After) |
New Bending Fixture Implemented. 518_Occurance_After.png |
Outflow (Before) |
Only Pin was guided as a reference in the block. 518_Outflow_Before.jpg |
Outflow (After) |
New Checking Fixture Made w.r.t Pin angle , pin shifting , part profile and connector angle concept. 518_Outflow_After.pdf |
11. Horizontal Deployment
Horizontal Deployment Required | No |
Applicable Machine / Model / Plant | Presently Only single model is there. |
12. Document Review
Documents | |
Specify Other Document | OPL |
13. Effectiveness Of Action
Reviewed Quantity | 300 |
Reason for submission | Lug ok observed in corrected lot |