QFR No - 8000839779
Defect Details
NC No. 8000839779
NC Date 08/08/2023
NC Submission Date
Part No. B2EH08502O
Part Name END CONNECTOR MASTER SIDE NTORQ
Supplier Name & Code 101221-SUNREN AUTOMOTIVE PRIVATE LIMI
ETL Plant 1120-ETL K-226/2 Disc Brakes
Defect Details OTHER-LUG NOT OK
 
1. Problem Description
Defect Description LUG NOT OK
Detection Stage Receipt
Problem Severity Fitment
NG Quantity 1359
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID shivank@sunren.in
Plant Head/CEO Email ID dharmbir@sunren.in
MD Email ID subhashsaini@sunren.in
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
0
17000
9000
2000
3000
31000
Check Qty
0
17000
9000
2000
3000
31000
NG Qty
0
243
0
0
0
243
 
Scrap 243
Rework 0
Under Deviation 0
Containment Action
100% inspection will be carried out at warehouse and green dot marking is placed over the lug for ensurity.
 
3. Process Flow
Process Flow Description
Inspection of Raw Material - Cutting Multi Operation - Centerless Grinding - Milling - Cross Drill - Neck Drill-Cross Reamer - Pin Drill - Pin Assembly - Brazing - Facing1st - Facing-2nd -Chamfer- 100% Visual Inspection -Bending - Plating - Final Inspection - Packaging - Storage / Dispatch .
 
4. Process Details
Process / Operation Bending
Outsource No
Machine / Cell Bending Fixture
Machine / Cell No. 10
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ManLack of KnowledgeSkill MatrixO
MethodInspection Method Not EffectiveGauge VerificationX
Toolwear and tear of fixturesFixture ValidationX
 
6. Inspection Method Analysis (Current)
Inspection Method Sp. Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 5
7. Root Cause Analysis (Occurance)
Why 1 wear & tear of bending fixture
Why 2 Fixture was not hardened
Why 3 Fixture life was not decided
Why 4 Fixture not validated
Why 5 Lack of awareness
Root Cause (Occurance) Wear & Tear of bending fixture
 
Root Cause Analysis (Outflow)
Why 1 Inspection process not effective
Why 2 Checking Gauge found not effective
Why 3 complete profile of the part was not covered in gauge
Why 4 Gauge Design Needs improvement
Why 5 Gauge Design not validated
Root Cause (Outflow) Checking Gauge Found Not Effective.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceFixture will be replaced , Hardened , Gauge validation will be done and improvement will be done in bending fixture taking pin as a reference for bending.Shivank29/09/202310/09/2023Completed
OutflowChecking gauge will be re-designed considering pin shifting , part profile and pin angle.Shivank29/09/202327/09/2023Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Lug shift is checked 200% and green dot marking is started over the lug for ensurity.
Inspection Method Sp. Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 5
10. Evidance of Countermeasure
Occurance (Before) Fixture Gets Wear and Tear.
518_Occurance_Before.png
Occurance (After) New Bending Fixture Implemented.
518_Occurance_After.png
Outflow (Before) Only Pin was guided as a reference in the block.
518_Outflow_Before.jpg
Outflow (After) New Checking Fixture Made w.r.t Pin angle , pin shifting , part profile and connector angle concept.
518_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant Presently Only single model is there.
 
12. Document Review
Documents
Specify Other Document OPL
 
13. Effectiveness Of Action
Reviewed Quantity 300
Reason for submission Lug ok observed in corrected lot