QFR No - 8000839822
Defect Details
NC No. | 8000839822 |
NC Date | 08/08/2023 |
NC Submission Date | |
Part No. | B2EH06002O |
Part Name | END CONNECTOR CAL SIDE N360 NON ABS |
Supplier Name & Code | 101221-SUNREN AUTOMOTIVE PRIVATE LIMI |
ETL Plant | 1120-ETL K-226/2 Disc Brakes |
Defect Details | PLATING NOT OK-PLATING NOT OK |
1. Problem Description
Defect Description | PLATING NOT OK |
Detection Stage | Receipt |
Problem Severity | Function |
NG Quantity | 33 |
Is Defect Repeatative? | No |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | shivank@sunren.in |
Plant Head/CEO Email ID | dharmbir@sunren.in |
MD Email ID | subhashsaini@sunren.in |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
0
|
2500
|
4000
|
1000
|
2000
|
9500
|
Check Qty |
0
|
2500
|
4000
|
1000
|
2000
|
9500
|
NG Qty |
0
|
0
|
0
|
22
|
0
|
22
|
Scrap | 0 |
Rework | 22 |
Under Deviation | 0 |
Containment Action |
---|
Re-Plating |
3. Process Flow
Process Flow Description |
---|
Raw Inspection of Raw Material - Cutting Multi Operation - Centerless Grinding - Milling - Cross Drill- Facing1st - Facing-2nd - Neck Drill-Cross Reamer - Chamfer- 100% Visual Inspection -Bending - Plating - Final Inspection - Packaging - Storage / Dispatch . |
4. Process Details
Process / Operation | Plating |
Outsource | Yes |
Machine / Cell | 01 |
Machine / Cell No. | 01 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Method | Jig was partially loaded | Jig was verified | X |
Man | Operator Negligency | Skill Level verified as per skill matrix | O |
6. Inspection Method Analysis (Current)
Inspection Method | Instrument |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 2 |
7. Root Cause Analysis (Occurance)
Why 1 | current distribution on part during plating process NG |
Why 2 | Jigs was partially loaded by operator |
Why 3 | SOP available but process not running as per defined SOP |
Why 4 | Operator skill level not found as per the SOP |
Why 5 | Training provided to the operator as per the SOP |
Root Cause (Occurance) | Jig was partially loaded with the EC. |
Root Cause Analysis (Outflow)
Why 1 | Material cannot be checked 100% |
Why 2 | Due to destructive testing |
Why 3 | |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | Material cannot be checked 100% due to destructive testing . |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Outflow | will check 2 parts by the use of plier . | Krishna Plating | 10/08/2023 | 10/08/2023 | Completed |
Occurance | OPL displayed for partial loading of Jigs | Krishna Plating | 10/08/2023 | 10/08/2023 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | Will check 02 Nos with the use of plier |
Inspection Method | Instrument |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 2 |
10. Evidance of Countermeasure
Occurance (Before) |
N/A 523_Occurance_Before.jpg |
Occurance (After) |
OPL Displayed 523_Occurance_After.jpg |
Outflow (Before) |
No mechanism to check peel off. 523_Outflow_Before.png |
Outflow (After) |
2 Nos/lot will be checked with the use of plier . 523_Outflow_After.png |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | B20706100,B20706200O,B20706300,B20703700O,B20703800O,B20703900,B2EH08502O,B2EH08602O,B2EH05902O,B20702500O,B20702700,B20707500O,B20707800O,B20708000O,B20708200O,B20708300OB2EH00802O |
12. Document Review
Documents | |
Specify Other Document | OPL |
13. Effectiveness Of Action
Reviewed Quantity | 500 |
Reason for submission | No plating defect found in latest lot |