QFR No - 8000839822
Defect Details
NC No. 8000839822
NC Date 08/08/2023
NC Submission Date
Part No. B2EH06002O
Part Name END CONNECTOR CAL SIDE N360 NON ABS
Supplier Name & Code 101221-SUNREN AUTOMOTIVE PRIVATE LIMI
ETL Plant 1120-ETL K-226/2 Disc Brakes
Defect Details PLATING NOT OK-PLATING NOT OK
 
1. Problem Description
Defect Description PLATING NOT OK
Detection Stage Receipt
Problem Severity Function
NG Quantity 33
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID shivank@sunren.in
Plant Head/CEO Email ID dharmbir@sunren.in
MD Email ID subhashsaini@sunren.in
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
0
2500
4000
1000
2000
9500
Check Qty
0
2500
4000
1000
2000
9500
NG Qty
0
0
0
22
0
22
 
Scrap 0
Rework 22
Under Deviation 0
Containment Action
Re-Plating
 
3. Process Flow
Process Flow Description
Raw Inspection of Raw Material - Cutting Multi Operation - Centerless Grinding - Milling - Cross Drill- Facing1st - Facing-2nd - Neck Drill-Cross Reamer - Chamfer- 100% Visual Inspection -Bending - Plating - Final Inspection - Packaging - Storage / Dispatch .
 
4. Process Details
Process / Operation Plating
Outsource Yes
Machine / Cell 01
Machine / Cell No. 01
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodJig was partially loadedJig was verifiedX
ManOperator NegligencySkill Level verified as per skill matrixO
 
6. Inspection Method Analysis (Current)
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 2
7. Root Cause Analysis (Occurance)
Why 1 current distribution on part during plating process NG
Why 2 Jigs was partially loaded by operator
Why 3 SOP available but process not running as per defined SOP
Why 4 Operator skill level not found as per the SOP
Why 5 Training provided to the operator as per the SOP
Root Cause (Occurance) Jig was partially loaded with the EC.
 
Root Cause Analysis (Outflow)
Why 1 Material cannot be checked 100%
Why 2 Due to destructive testing
Why 3
Why 4
Why 5
Root Cause (Outflow) Material cannot be checked 100% due to destructive testing .
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
Outflowwill check 2 parts by the use of plier .Krishna Plating10/08/202310/08/2023Completed
OccuranceOPL displayed for partial loading of JigsKrishna Plating10/08/202310/08/2023Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Will check 02 Nos with the use of plier
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 2
10. Evidance of Countermeasure
Occurance (Before) N/A
523_Occurance_Before.jpg
Occurance (After) OPL Displayed
523_Occurance_After.jpg
Outflow (Before) No mechanism to check peel off.
523_Outflow_Before.png
Outflow (After) 2 Nos/lot will be checked with the use of plier .
523_Outflow_After.png
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant B20706100,B20706200O,B20706300,B20703700O,B20703800O,B20703900,B2EH08502O,B2EH08602O,B2EH05902O,B20702500O,B20702700,B20707500O,B20707800O,B20708000O,B20708200O,B20708300OB2EH00802O
 
12. Document Review
Documents
Specify Other Document OPL
 
13. Effectiveness Of Action
Reviewed Quantity 500
Reason for submission No plating defect found in latest lot