QFR No - 8000843595
Defect Details
NC No. | 8000843595 |
NC Date | 07/09/2023 |
NC Submission Date | |
Part No. | B2GQ01903O |
Part Name | MASTER CYLINDER RAW CASTING- C101 H |
Supplier Name & Code | 100398-MANOJ INDUSTRIES |
ETL Plant | 1120-ETL K-226/2 Disc Brakes |
Defect Details | BLOW HOLES-LEAKAGE AT CUSTOMER END |
1. Problem Description
Defect Description | Leakage |
Detection Stage | Customer End |
Problem Severity | Safety |
NG Quantity | 1 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | qad@manojindustrieskop.com |
Plant Head/CEO Email ID | foundry@manojindustrieskop.com |
MD Email ID | mgnt@manojindustrieskop.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
1300
|
0
|
0
|
0
|
0
|
1300
|
Check Qty |
1300
|
0
|
0
|
0
|
0
|
1300
|
NG Qty |
1
|
0
|
0
|
0
|
0
|
1
|
Scrap | 1 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
---- |
3. Process Flow
Process Flow Description |
---|
Casting production |
4. Process Details
Process / Operation | Casting production |
Outsource | No |
Machine / Cell | MI Tilt -19 |
Machine / Cell No. | MI Tilt -19 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | Die modification |
Check Point at Final Inspection | No |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
7. Root Cause Analysis (Occurance)
Why 1 | Leakage observed at customer end. |
Why 2 | Shrinkage porosity observed at below barrel OD at corner radius |
Why 3 | Improper feeding of material at barrel OD area |
Why 4 | Due to cross sectional variation shrinkage porosity observed. |
Why 5 | |
Root Cause (Occurance) | Due to cross sectional variation shrinkage porosity observed. |
Root Cause Analysis (Outflow)
Why 1 | Leakage observed at customer end. |
Why 2 | Defect not seen by nacked eyes |
Why 3 | |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | --- |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | We are adding extra feeder as per proposed action it will help to feed the casting below lug area | D B LAD | 21/09/2023 | 29/09/2023 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | No |
Change Details | no change |
Inspection Method | Other |
Other Inspection Method | DP test done |
Check Point at Final Inspection | No |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | daily |
10. Evidance of Countermeasure
Occurance (Before) |
Leakage observed at bellow lug area 542_Occurance_Before.png |
Occurance (After) |
We are adding extra feeder as per proposed action it will help to feed the casting below lug area 542_Occurance_After.png |
Outflow (Before) |
Leakage observed at bellow lug area 542_Outflow_Before.png |
Outflow (After) |
--- 542_Outflow_After.png |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | All C101 master cyl |
12. Document Review
Documents | |
Specify Other Document | no |
13. Effectiveness Of Action
Reviewed Quantity | 500 |
Reason for submission | NO leakage found in received lot |