QFR No - 8000843758
Defect Details
NC No. 8000843758
NC Date 08/09/2023
NC Submission Date
Part No. F800500507
Part Name UNDER BRACKET ASSEMBLY
Supplier Name & Code 100060-A.G.TRANSMISSIONS
ETL Plant 1117-ETL K-228/9 Suspension
Defect Details PAINT PEEL OFF-
 
1. Problem Description
Defect Description Under bracket powder coating peel off
Detection Stage Customer End
Problem Severity Aesthetic
NG Quantity 80
Is Defect Repeatative? No
Defect Sketch / Photo pb5pwowhm0lnevbbhi3i5h1c.pdf
Supplier Communication Details
Quality Head Email ID agtransmissions@rediffmail.com
Plant Head/CEO Email ID agforge@rediffmail.com
MD Email ID agtransmissions@rediffmail.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
677
3346
0
1800
749
6572
Check Qty
677
3346
0
1800
749
6572
NG Qty
677
11
0
11
7
706
 
Scrap 0
Rework 706
Under Deviation 0
Containment Action
AGT has recalled suspected lot i.e. 677 Nos. & remaining parts are kept on hold
 
3. Process Flow
Process Flow Description
Forging Incoming, Bracket Machining, Shaft Machining, Insert Pressing & welding, Shaft Machining, Assembly Welding, Powder Coating, Tapping, Fine Boring, Final Inspection
 
4. Process Details
Process / Operation Powder Coating
Outsource No
Machine / Cell Powder Coating setup
Machine / Cell No. Powder Coating
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ManOperator unskilledSkill Matrix availableO
ManOperation skip by operatorProcess flow followed by operatorO
ManAssembly not dip properlyMay assembly not dip properly.O
MethodInlet and Outlet FRL cleaning is not maintainedInlet and Outlet FRL cleaning is maintainedO
MethodPre Heating Not donePre Heating doneO
MethodTitration Not doneTitration doneO
MethodAfter PT process part not cleaningAfter PT process part cleaningO
MaterialAlkaline Degresing PointageAlkaline Degresing Pointage okO
MaterialWater ringing PH 2 no.Water ringing PH 2 no. okO
MaterialActivation PHActivation PH okO
MaterialPassivation PointagePassivation Pointage okO
MaterialAll titration solution not availableAll titration solution availableO
MaterialHigher / lower DFTDFT IS OKO
MachinePM of PC gun not donePM of PC gun doneO
MachineCompressor not drain or dryer not workingCompressor is drain or dryer workingO
MachineP.C machine programm changeP.C machine program not change (program passed protected)O
MachineOven PM not doneOven PM not doneO
MachineTTR not okTTR not okX
MachineOil skimmer not workingOil skimmer workingO
MachineAll timer not workingAll timer workingO
MachineAll sensors are not workingAll sensors are workingO
MachineAll timer Buzzers not workingAll timer Buzzers workingO
MachineAll tank Air agitationAll tank Air agitationO
MachineTank Temperature not OKTank Temperature okO
MachineOil not removed in the PT processOil removed in the PT processO
ManPT process inspection awarenessAware of PT process inspectionO
MaterialDegressing & derusting PointageDegressing & derusting Pointage okO
MaterialWater rinsing PH 4 no.Water rinsing PH 4 no.okO
MethodPowder Coating Gun cleaning frequencyPowder Coating Gun cleaning frequency flowedO
MaterialPhospating pointagePhospating pointage okO
MethodTank top up frequency not followedTank top up frequency followedO
MaterialWatrer Rinsing PH 7Watrer Rinsing PH 7 okO
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method By Hammering method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size After 20 n
7. Root Cause Analysis (Occurance)
Why 1 Peel off observed at customer end
Why 2 Uneven Temp. in Oven.
Why 3 TTR was done 6 months ago as per defined frequency.
Why 4
Why 5
Root Cause (Occurance) TTR was done 6 months ago as per defined frequency.
 
Root Cause Analysis (Outflow)
Why 1 Scratch test and rubber hammer test found ok
Why 2 Both test carried out after 2hour of powder coating work
Why 3 Lack of knowledge and awareness of the powder coating test
Why 4
Why 5
Root Cause (Outflow) Lack of knowledge and awareness of the powder coating test
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceTTR frequency modified to Per month.QA21/09/202327/09/2023Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 100% Inspection started by Hammering method
Inspection Method Other
Other Inspection Method By Hammering & Visua
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) TTR was done 6 months ago as per defined frequency.
543_Occurance_Before.pdf
Occurance (After) TTR frequency decided one moth
543_Occurance_After.pdf
Outflow (Before) Inspection done after 20 no`s job by hammering and visual
543_Outflow_Before.xlsx
Outflow (After) 100% hammering and inspection done
543_Outflow_After.xlsx
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant only One Oven in company primises
 
12. Document Review
Documents WISOP
Specify Other Document TTR plan
 
13. Effectiveness Of Action
Reviewed Quantity 150
Reason for submission 3 different lots of different model verified and found ok