QFR No - 8000844147
Defect Details
NC No. | 8000844147 |
NC Date | 12/09/2023 |
NC Submission Date | |
Part No. | 520FZ01002 |
Part Name | HUB CLUTCH WITH INNER RING REML 6/7 PL |
Supplier Name & Code | 100656-MADHURA DIE CAST PVT.LTD |
ETL Plant | 1132-ETL K-226/1 TRANSMISSION |
Defect Details | NOT AS PER SPECIFICATION-RING LOOSE |
1. Problem Description
Defect Description | Warranty complaint -Ring Loose issue in Hub Clutch |
Detection Stage | Warranty |
Problem Severity | Function |
NG Quantity | 1 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | madhuradiecast@gmail.com |
Plant Head/CEO Email ID | madhuradiecast@gmail.com |
MD Email ID | madhuradiecast@gaikegroup.in |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
500
|
1000
|
0
|
500
|
300
|
2300
|
Check Qty |
500
|
1000
|
0
|
500
|
300
|
2300
|
NG Qty |
1
|
0
|
0
|
0
|
0
|
1
|
Scrap | 1 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
100% segregation done at customer End & Supplier End. |
3. Process Flow
Process Flow Description |
---|
1.Casting 2.fetling 3. CNC 1st Set-up 4.CNC 2nd Set-up 5. Ring Pressing 6.Broaching 7. CNC OD Turning 6.Final Inspection |
4. Process Details
Process / Operation | CNC |
Outsource | No |
Machine / Cell | CNC 2 ND SET UP |
Machine / Cell No. | 06 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Method | Due to overheated which inner ring id got expanded. | verified & found not ok | X |
Tool | Jaw loose in running | Check and verify found ok | O |
Man | Unskilled operator was operate machine | Skill Matrix is verified & found ok | O |
Material | Burr on clamping area | Verify the component found ok | O |
6. Inspection Method Analysis (Current)
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 1:1 |
7. Root Cause Analysis (Occurance)
Why 1 | Ring Loose issue in Hub Clutch |
Why 2 | Ring inner dia increased by 0.031 mm & outer dia increased by 0.022 mm |
Why 3 | The Mating part (Bearing) resting on inner ring od got seized . |
Why 4 | Due to overheated which inner ring id got expanded |
Why 5 | |
Root Cause (Occurance) | Due to overheated which inner ring id got expanded |
Root Cause Analysis (Outflow)
Why 1 | Ring Loose issue in Hub Clutch |
Why 2 | 100% inspection not done at all stages |
Why 3 | |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | 100% inspection not done at all stages |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Outflow | 1. 100% inner ring id checking started at inward inspection with air gauge. 2. 100% id inspection with air gauge at load cell stage before ring pressing. 3. 100% inspection of inner ring outer dia at CNC Stage after grinding. 4. 100% inspection of inner ring outer dia at final inspection stage before dispatch. | Quality Supervisor | 15/10/2023 | 09/10/2023 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | started 100% inner ring id & od Inspection at all stages |
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 1:1 |
10. Evidance of Countermeasure
Occurance (Before) |
Action plan PPT is attached for this problem 551_Occurance_Before.pptx |
Occurance (After) |
For complete root cause action & analysis we need to checked mating part(bearing) which is resting on inner ring OD 551_Occurance_After.jpg |
Outflow (Before) |
100% inspection not done at all stages 551_Outflow_Before.xls |
Outflow (After) |
1. 100% inner ring id checking started at inward inspection with air gauge. 2. 100% id inspection with air gauge at load cell stage before ring pressing. 3. 100% inspection of inner ring outer dia at CNC Stage after grinding. 4. 100% inspection of inner ring outer dia at final inspection stage before dispatch. 551_Outflow_After.xls |
11. Horizontal Deployment
Horizontal Deployment Required | No |
Applicable Machine / Model / Plant | CNC |
12. Document Review
Documents | ControlPlan, PFMEA, InspCheckSheet |
Specify Other Document | QA ALERT |
13. Effectiveness Of Action
Reviewed Quantity | |
Reason for submission |