QFR No - 8000847104
Defect Details
NC No. 8000847104
NC Date 03/10/2023
NC Submission Date
Part No. 520PP01902
Part Name WHEEL CLUTCH FINISHED UPGRADE
Supplier Name & Code 100656-MADHURA DIE CAST PVT.LTD
ETL Plant 1132-ETL K-226/1 TRANSMISSION
Defect Details RUN OUT MORE-FITMNET ISSUE DUE TO TEETH R/O UPTO 1 MM
 
1. Problem Description
Defect Description Customer Return -Fitment issue due to teeth run out found up to 1.15 mm against 0.2 mm
Detection Stage Customer End
Problem Severity Fitment
NG Quantity 2
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID madhuradiecast@gmail.com
Plant Head/CEO Email ID madhuradiecast@gmail.com
MD Email ID madhuradiecast@gaikegroup.in
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
1000
0
0
500
600
2100
Check Qty
1000
0
0
500
600
2100
NG Qty
2
0
0
1
1
4
 
Scrap 4
Rework 0
Under Deviation 0
Containment Action
100% SEGERATION DONE AT SUPPLIER END STARTED BLUE IDENTIFICATION DOT MARK ON COMPONENTS
 
3. Process Flow
Process Flow Description
1.Casting 2.fetling 3. CNC 1st Set-up 4.CNC 2nd Set-up 5.Drilling & Tapping 6.Final Inspection
 
4. Process Details
Process / Operation CNC 1ST Set-up
Outsource No
Machine / Cell CNC
Machine / Cell No. 06
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ManUnskill operator operate machineSkill matrix verify found okO
MaterialWrong grade Material is usedVerified & Found OKO
MethodInput & output material bin not identified on CNC stageVerified & Found okO
MachineJaw clamping pad area in CNC chuck got wearFound Not OKX
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 1:1
7. Root Cause Analysis (Occurance)
Why 1 Fitment issue due to teeth run out found up to 1.15 mm against 0.2 mm
Why 2 CNC machine chuck Jaw abnormal clamping
Why 3 out of three one jaw got play during clamping
Why 4 Jaw clamping pad area in CNC chuck got wear
Why 5 Jaw clamping area play found upto 0.15 mm.
Root Cause (Occurance) Jaw clamping pad area in CNC chuck got wear
 
Root Cause Analysis (Outflow)
Why 1 Fitment issue due to teeth run out found up to 1.15 mm against 0.2 mm
Why 2 Teeth Runout checking not checking at Final stage
Why 3
Why 4
Why 5
Root Cause (Outflow) Teeth Runout checking not checking at Final stage
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
Outflow1. Started 100% Inspection with attribute type teeth runout Checking gauge at Final stage. 2. Also Fitment checking parameter with meeting part 3W4S hub added in final inspection check sheet. 3. Inspection Agreement & PDIR is revised for 100% inspection with attribute type teeth runout gauge. 4. Started doc audit daily basis & data maintained .Quality Supervisor05/10/202305/10/2023Completed
Occurance1.New chuck is provided & old chuck is send for reconditioning . 2.Started Jaw Clamping (Working condition ) Verification on daily JH Activity . 3.PM Plan revised Mentioned specific dimension of chuck guide area 14 mm tolerance upto, +H7(0.025mm). 4.Started Chuck Inspection by using master Ring & dial stand point verified in daily JH activity. 5.Jaw Boring frequency is define in PM Check sheet & its monitoring started. 6.Clamping pressure validation started interlock given to chuck clamping pressure. 7.New attribute Relation gauge manufacturing is started . Mgf .Target Date – 05.11.2023 8.Customer complain action sustenance verification register maintain.9.Special Jaw Chuck to be implemented at CNC Machining to avoid part shift & Achieve teeth runout .Production Supervisor15/10/202305/10/2023Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Started 100% Inspection with attribute type teeth runout Checking gauge at Final stage. Also Fitment checking parameter with meeting part 3W4S hub added in final inspection check sheet.
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 1:10
10. Evidance of Countermeasure
Occurance (Before) Jaw clamping pad area in CNC chuck got wear
561_Occurance_Before.jpg
Occurance (After) .1.New chuck is provided & old chuck is send for reconditioning . 2.Started Jaw Clamping (Working condition ) Verification on daily JH Activity . 3.PM Plan revised Mentioned specific dimension of chuck guide area 14 mm tolerance upto, +H7(0.025mm). 4.Started Chuck Inspection by using master Ring & dial stand point verified in daily JH activity. 5.Jaw Boring frequency is define in PM Check sheet & its monitoring started. 6.Clamping pressure validation started interlock given to chuck clamping pressure. 7.New attribute Relation gauge manufacturing is started . Mgf .Target Date – 05.11.2023 8.Customer complain action sustenance verification register maintain.9.Special Jaw Chuck to be implemented at CNC Machining to avoid part shift & Achieve teeth runout .
561_Occurance_After.xlsx
Outflow (Before) Teeth Runout checking not checking at Final stage
561_Outflow_Before.mp4
Outflow (After) Started 100% Inspection with attribute type teeth runout Checking gauge at Final stage. Also Fitment checking parameter with meeting part 3W4S hub added in final inspection check sheet.
561_Outflow_After.jfif
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant 3W4S WHEEL CLUTCH FINISHED UPGRADE
 
12. Document Review
Documents ControlPlan, PMCheckSheet, PFMEA, JHCheckSheet, InspCheckSheet
Specify Other Document NO
 
13. Effectiveness Of Action
Reviewed Quantity 10000
Reason for submission OK