QFR No - 8000851178
Defect Details
NC No. 8000851178
NC Date 06/11/2023
NC Submission Date
Part No. 550LG06702
Part Name SEAT PIPE-(HMS-30 & HMP-30)
Supplier Name & Code 100538-NARINDER PARKASH AND CO
ETL Plant 1143-ETL Suspension Halol, Vadodara
Defect Details NOT AS PER SPECIFICATION-HALF THREAD
 
1. Problem Description
Defect Description Seat Pipe M8 X 1.25 -6G half thread and Thread Length Short
Detection Stage Inprocess
Problem Severity Function
NG Quantity 1
Is Defect Repeatative? No
Defect Sketch / Photo f3flbtnxltmnvijxhuriho0h.jpg
Supplier Communication Details
Quality Head Email ID quality@npcindustries.in
Plant Head/CEO Email ID anand@npcindustries.in
MD Email ID ajay@npcindustries.in
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
3800
8200
0
0
0
12000
Check Qty
3800
8200
0
0
0
12000
NG Qty
2
0
0
0
0
2
 
Scrap 2
Rework 0
Under Deviation 0
Containment Action
Thread length checking with thread plug gauge.
 
3. Process Flow
Process Flow Description
Raw material Inspection - Cutting - Draw - Forging - Rough Grinding - Punching - CNC Head turning - CNC Tail facing - Tapping & Chamfering - Final Inspection - Cleaning - Oiling - Packing & Dispatch
 
4. Process Details
Process / Operation Tapping
Outsource No
Machine / Cell Tapping machine
Machine / Cell No. TM-03
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodIncorrect location of part during TappingAfter verification we found part was located at Incorrect location.X
ManOperator negligenceAfter verification we found operator was aware about processO
MaterialMaterial HardAfter verification we found material was used as per std.O
ToolWrong tapping tool useAfter verification we found tapping tool was used as per std.O
MachineTap tightening not okAfter verification we found tap tightening was okO
 
6. Inspection Method Analysis (Current)
Inspection Method Sp. Gauge
Other Inspection Method
Check Point at Final Inspection No
Checking Freq. Sampling
Sampling No
Sample Size As per std
7. Root Cause Analysis (Occurance)
Why 1 Half thread seatpipe found
Why 2 part was located at Incorrect location.
Why 3 The part was setted below the specified location
Why 4 No reference available on Fixture
Why 5 there was not available any stopper.
Root Cause (Occurance) there is not available any stopper.
 
Root Cause Analysis (Outflow)
Why 1 Half thread seatpipe found
Why 2 Could not be detected at Final Inspection
Why 3 Skipped in sampling at Final Inspection
Why 4 Sampling quantity was less.
Why 5
Root Cause (Outflow) Sampling quantity was less.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceNew clamp fixture to be modified with stopper.Mr Ravinder Singh10/11/202309/11/2023Completed
OutflowSampling quantity to be increased.Mr. Ankush08/11/202307/11/2023Completed
OccuranceQuality Alert to be displayed at working stationMr. Princ07/11/202306/11/2023Completed
OutflowQuality alert to be displayed at final Q- inspection stationMr. Princ07/11/202306/11/2023Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details sampling quantity to be doubled at final inspection station.
Inspection Method Sp. Gauge
Other Inspection Method
Check Point at Final Inspection No
Checking Freq. Sampling
Sampling No
Sample Size double
10. Evidance of Countermeasure
Occurance (Before) No stopper was available in clamp fixture
588_Occurance_Before.png
Occurance (After) New clamp fixture to be modified with stopper.
588_Occurance_After.png
Outflow (Before) Quality alert not available at final inspection. Sampling qty was less.
588_Outflow_Before.jpg
Outflow (After) Display quality alert at work station & final Q-gate. Samling qty to be double.
588_Outflow_After.png
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant Tapping machine
 
12. Document Review
Documents ControlPlan, PFMEA, WISOP, InspCheckSheet
Specify Other Document Not required
 
13. Effectiveness Of Action
Reviewed Quantity 50
Reason for submission ok