QFR No - 8000851228
Defect Details
NC No. 8000851228
NC Date 07/11/2023
NC Submission Date
Part No. 165FZ00322
Part Name HUB CLUTCH BROACHED JW/BM-150
Supplier Name & Code 101100-CAST 4 ALUMINIUM PVT LTD
ETL Plant 1132-ETL K-226/1 TRANSMISSION
Defect Details CRACKS-CRACK ISSUE
 
1. Problem Description
Defect Description Hub Clutch observed crack (Repeated occurrence )
Detection Stage Inprocess
Problem Severity Function
NG Quantity 2
Is Defect Repeatative? Yes
Defect Sketch / Photo h1etbmobscijlsy1xp32ecw3.jpg
Supplier Communication Details
Quality Head Email ID info@cast4aluminium.com
Plant Head/CEO Email ID info@cast4aluminium.com
MD Email ID kiran@cast4aluminium.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
2268
0
0
7000
0
9268
Check Qty
2268
0
0
7000
0
9268
NG Qty
4
0
0
7
0
11
 
Scrap 11
Rework 0
Under Deviation 0
Containment Action
Segregation done for 7000 nos of JW hub at cast 4 end from which 7 parts are found for crack.
 
3. Process Flow
Process Flow Description
RM--->Melting--->Cleaning--->Cleaning--->PDC
 
4. Process Details
Process / Operation PDC
Outsource No
Machine / Cell PDC Machine
Machine / Cell No. PDC M/C No.
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ToolErosion markYes, possibleO
MachineExcess clamping pressure of CNC ChuckYes, possibleO
ToolScoring mark on dieYes, possibleO
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visual Inspection
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 Crack Observed on the friction face of JW Hub.
Why 2 Cracks observed at same position i.e. on the Gate Area side and in the cavity no. 3 only.
Why 3 Casting was getting stuck in the die while ejecting .
Why 4 Scoring observed in the die and excess rubbing mark observed on the part.
Why 5 Erosion mark observed near gate area & scoring on die.
Root Cause (Occurance) Erosion mark observed near gate area & scoring on die.
 
Root Cause Analysis (Outflow)
Why 1 Crack part found at ETL.
Why 2 Crack was not identified by the two inspectors only.
Why 3 Training was given to all of the inspectors still these two inspector was not able to detect the crack part.
Why 4 Training effectiveness was not monitored
Why 5
Root Cause (Outflow) Training effectiveness was not monitored
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
Occurance1. Die polishing done while PM. 2. New die planning will be done on the priority basis.1. Die maint. team 2. Top management17/11/202317/11/2023Completed
Outflow1. One Point lesson displayed and training given to the inspectors 2. Training effectiveness monitoring for these two inspectors will be planed. 4. For crack checking special marking is given. 5.Part is being checked under the magnifying glass 6.DP test on the gate area will be done on the sampling basis.Mr. Qasim10/11/202310/11/2023Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Part is being checked under the magnifying glass
Inspection Method Other
Other Inspection Method Visual Inpection
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Scoring mark on die
590_Occurance_Before.png
Occurance (After) Die polishing done while PM.
590_Occurance_After.jpeg
Outflow (Before) NA
590_Outflow_Before.png
Outflow (After) Part is being checked under the magnifying glass
590_Outflow_After.png
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant NA
 
12. Document Review
Documents PMCheckSheet, PFMEA, WISOP
Specify Other Document NA
 
13. Effectiveness Of Action
Reviewed Quantity 1000
Reason for submission OK