QFR No - 8000851574
Defect Details
NC No. 8000851574
NC Date 10/11/2023
NC Submission Date
Part No. F2LG05402B
Part Name SEAT PIPE - J1A & J1D
Supplier Name & Code 100539-N P ENTERPRISES
ETL Plant 1117-ETL K-228/9 Suspension
Defect Details NOT AS PER SPECIFICATION-ID STEP, OD GRROVE STEP
 
1. Problem Description
Defect Description Step observed in head groove
Detection Stage Inprocess
Problem Severity Function
NG Quantity 82
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID quality@npcindustries.in
Plant Head/CEO Email ID anand@npcindustries.in
MD Email ID ajay@npcindustries.in
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
58240
60000
18000
0
0
136240
Check Qty
58158
59990
18000
0
0
136148
NG Qty
82
10
0
0
0
92
 
Scrap 92
Rework 0
Under Deviation 0
Containment Action
segregate all material
 
3. Process Flow
Process Flow Description
Cutting - Draw - Forging - Rough Grinding - Punching - CNC Head Turning - CNC Tail Facing - Tapping & Chamfering - Final Grinding - Final Inspection - Cleaning - RPO Oiling - Packing & Dispatch.
 
4. Process Details
Process / Operation CNC Head Turning
Outsource No
Machine / Cell CNC
Machine / Cell No. CNC - 07
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodVariation during part loadingAfter verification we found No variation observed during part loadingO
ToolWorn out Head Forging Punch PinAfter verification we observed usage of worn out Punch Pin results in step markX
MachineCNC program temperedAfter verification we found CNC program was not tamperedO
ToolCNC insert fitment NGAfter verification we found CNC insert was DislocateX
ManOperator unskilledAfter verification we found Operator observed to be skilledO
MaterialOther grade material useAfter verification we found Material was used as per define std.O
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection No
Checking Freq. Sampling
Sampling No
Sample Size as per std
7. Root Cause Analysis (Occurance)
Why 1 Step in Hex ID and step in Groove OD surface.
Why 2 Worn out Punch not changed at forging & Variation in size during CNC Turning .
Why 3 Punch change frequency followed at forging & Dislocation of the Turning tool bit at CNC.
Why 4 Punch change frequency not adequate at forging & Turning tool bit loose.
Why 5
Root Cause (Occurance) 1. Punch change frequency not adequate at forging 2. Turning tool bit loose.
 
Root Cause Analysis (Outflow)
Why 1 Step in Hex ID and step in Groove OD surface.
Why 2 Could not be detected at Final inspection
Why 3 Skipped in Sampling at Final Inspection
Why 4 Sampling Quantity was inadequate
Why 5
Root Cause (Outflow) Sampling Quantity was inadequate
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OutflowQ- alert to be displayed in Final inspection .Mr. Princ11/11/202311/11/2023Completed
OutflowNew snap gauge to be modified for detection of the groove width.Mr. Ravinder15/11/202312/11/2023Completed
OccuranceQ- alert to be displayed in Forging & CNC shop.Mr. Princ11/11/202311/11/2023Completed
Outflow100 % Inspection to be start with Visual & Snap Gauge at final inspection.Mr. Ankush14/11/202311/11/2023Completed
OccurancePunch change frequency to be revalidated and freezedMr. Narinder15/11/202315/11/2023Completed
OccuranceInsert tightening bolt inspection to be added in daily Startup checksheetMr. Princ15/11/202312/11/2023Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 100 % inspection start
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) No any checkpoint available in daily Startup checksheet
593_Occurance_Before.jpeg
Occurance (After) Insert tightening bolt inspection to be added in daily Startup checksheet
593_Occurance_After.png
Outflow (Before) Sampling plan follow at final inspection
593_Outflow_Before.jpg
Outflow (After) New snap gauge to be modified for detection of the groove width.
593_Outflow_After.png
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant CNC Machine
 
12. Document Review
Documents ControlPlan, WISOP, JHCheckSheet, InspCheckSheet
Specify Other Document Not Required
 
13. Effectiveness Of Action
Reviewed Quantity 280
Reason for submission All parts found ok during verificaction