QFR No - 8000852794
Defect Details
NC No. 8000852794
NC Date 24/11/2023
NC Submission Date
Part No. D3AD00500M
Part Name SHAFT CUT LENGTH (R122C MAXIMA Z)
Supplier Name & Code 101222-SANGKAJ ENGINEERING PVT LTD- U
ETL Plant 1152-ETL L-6/3/1DrivShaft
Defect Details LENGTH OVERSIZE-LENGTH O/S BY 1 TO 2MM
 
1. Problem Description
Defect Description Total Length Oversize by 1 to 2mm
Detection Stage Receipt
Problem Severity Function
NG Quantity 1000
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID irfan@sangkaj.com
Plant Head/CEO Email ID steel@sangkaj.com
MD Email ID anirudh.2007@hotmail.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
7000
0
0
800
0
7800
Check Qty
1005
0
0
10
0
1015
NG Qty
1000
0
0
10
0
1010
 
Scrap 0
Rework 1000
Under Deviation 0
Containment Action
Segregation Pipeline material at ETL end & pipeline In-house material.
 
3. Process Flow
Process Flow Description
Bar cutting- -Straightening -Grinding-final inspection- Packing -Dispatch
 
4. Process Details
Process / Operation Bar cutting
Outsource No
Machine / Cell Troub M/c
Machine / Cell No. 1
5. Problem Analysis
-------
Type Possible Cause Fact Verification Jud
 
6. Inspection Method Analysis (Current)
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection No
Checking Freq. Sampling
Sampling No
Sample Size 10 Nos per
7. Root Cause Analysis (Occurance)
Why 1 LENGTH OVERSIZE-LENGTH O/S BY 1 TO 2 MM
Why 2 Bar End pics mix-up in OK qty
Why 3 Bar End pics Area not defined
Why 4
Why 5
Root Cause (Occurance) Bar End pics Area not defined.
 
Root Cause Analysis (Outflow)
Why 1 LENGTH OVERSIZE-LENGTH O/S BY 1 TO 2 MM
Why 2 T.L Oversize not detect in Final inspection .
Why 3 Total Length Check as Sampling basis as per standard.
Why 4
Why 5
Root Cause (Outflow) Total Length Check as Sampling basis as per standard.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OutflowT.L C type Snap gauge provided to M/C&final inspection. T.L 100% check by C type Snap gaugeOperator /inspector04/12/202304/12/2023Completed
OccuranceBar End Pics Area defined.QA inspector29/11/2023Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details T.L C type Snap gauge provided to M/C . T.L 100% check by C type Snap gauge.
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection No
Checking Freq. 100%
Sampling No
Sample Size 100 %
10. Evidance of Countermeasure
Occurance (Before) Bar End pics Area not defined
599_Occurance_Before.jpeg
Occurance (After) Bar End pics Area defined
599_Occurance_After.jpeg
Outflow (Before) Total Length Check as Sampling basis as per standard by H.G.
599_Outflow_Before.jpeg
Outflow (After) T.L C type Snap gauge provided to final inspection. T.L 100% check by C type Snap gauge.
599_Outflow_After.jpeg
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant Man & Method
 
12. Document Review
Documents ControlPlan, PFMEA
Specify Other Document NO
 
13. Effectiveness Of Action
Reviewed Quantity
Reason for submission