QFR No - 8000852794
Defect Details
NC No. | 8000852794 |
NC Date | 24/11/2023 |
NC Submission Date | |
Part No. | D3AD00500M |
Part Name | SHAFT CUT LENGTH (R122C MAXIMA Z) |
Supplier Name & Code | 101222-SANGKAJ ENGINEERING PVT LTD- U |
ETL Plant | 1152-ETL L-6/3/1DrivShaft |
Defect Details | LENGTH OVERSIZE-LENGTH O/S BY 1 TO 2MM |
1. Problem Description
Defect Description | Total Length Oversize by 1 to 2mm |
Detection Stage | Receipt |
Problem Severity | Function |
NG Quantity | 1000 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | irfan@sangkaj.com |
Plant Head/CEO Email ID | steel@sangkaj.com |
MD Email ID | anirudh.2007@hotmail.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
7000
|
0
|
0
|
800
|
0
|
7800
|
Check Qty |
1005
|
0
|
0
|
10
|
0
|
1015
|
NG Qty |
1000
|
0
|
0
|
10
|
0
|
1010
|
Scrap | 0 |
Rework | 1000 |
Under Deviation | 0 |
Containment Action |
---|
Segregation Pipeline material at ETL end & pipeline In-house material. |
3. Process Flow
Process Flow Description |
---|
Bar cutting- -Straightening -Grinding-final inspection- Packing -Dispatch |
4. Process Details
Process / Operation | Bar cutting |
Outsource | No |
Machine / Cell | Troub M/c |
Machine / Cell No. | 1 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|
6. Inspection Method Analysis (Current)
Inspection Method | Instrument |
Other Inspection Method | |
Check Point at Final Inspection | No |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 10 Nos per |
7. Root Cause Analysis (Occurance)
Why 1 | LENGTH OVERSIZE-LENGTH O/S BY 1 TO 2 MM |
Why 2 | Bar End pics mix-up in OK qty |
Why 3 | Bar End pics Area not defined |
Why 4 | |
Why 5 | |
Root Cause (Occurance) | Bar End pics Area not defined. |
Root Cause Analysis (Outflow)
Why 1 | LENGTH OVERSIZE-LENGTH O/S BY 1 TO 2 MM |
Why 2 | T.L Oversize not detect in Final inspection . |
Why 3 | Total Length Check as Sampling basis as per standard. |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | Total Length Check as Sampling basis as per standard. |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Outflow | T.L C type Snap gauge provided to M/C&final inspection. T.L 100% check by C type Snap gauge | Operator /inspector | 04/12/2023 | 04/12/2023 | Completed |
Occurance | Bar End Pics Area defined. | QA inspector | 29/11/2023 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | T.L C type Snap gauge provided to M/C . T.L 100% check by C type Snap gauge. |
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | No |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100 % |
10. Evidance of Countermeasure
Occurance (Before) |
Bar End pics Area not defined 599_Occurance_Before.jpeg |
Occurance (After) |
Bar End pics Area defined 599_Occurance_After.jpeg |
Outflow (Before) |
Total Length Check as Sampling basis as per standard by H.G. 599_Outflow_Before.jpeg |
Outflow (After) |
T.L C type Snap gauge provided to final inspection. T.L 100% check by C type Snap gauge. 599_Outflow_After.jpeg |
11. Horizontal Deployment
Horizontal Deployment Required | No |
Applicable Machine / Model / Plant | Man & Method |
12. Document Review
Documents | ControlPlan, PFMEA |
Specify Other Document | NO |
13. Effectiveness Of Action
Reviewed Quantity | |
Reason for submission |