QFR No - 8000852795
Defect Details
NC No. | 8000852795 |
NC Date | 24/11/2023 |
NC Submission Date | |
Part No. | D3AD00500M |
Part Name | SHAFT CUT LENGTH (R122C MAXIMA Z) |
Supplier Name & Code | 101222-SANGKAJ ENGINEERING PVT LTD- U |
ETL Plant | 1152-ETL L-6/3/1DrivShaft |
Defect Details | DIAMETER OVER SIZE-OD O/S & SCRTCH MARK ON OD |
1. Problem Description
Defect Description | DIAMETER OVER SIZE-OD O/S & Taper & SCRTCH MARK ON OD - Shaft Maxima |
Detection Stage | Inprocess |
Problem Severity | Function |
NG Quantity | 514 |
Is Defect Repeatative? | No |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | Irfan@sangkaj.com |
Plant Head/CEO Email ID | steel@sangkaj.com |
MD Email ID | anirudh.2007@hotmail.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
7000
|
0
|
0
|
1000
|
0
|
8000
|
Check Qty |
4500
|
0
|
0
|
1000
|
0
|
5500
|
NG Qty |
514
|
0
|
0
|
0
|
0
|
514
|
Scrap | 0 |
Rework | 514 |
Under Deviation | 0 |
Containment Action |
---|
segregate pipe line material at ETL end & inhouse. |
3. Process Flow
Process Flow Description |
---|
BAR CUTTING- TURNING -STRAIGHTENING-GRINDING- FINAL INSPECTION-PACKING-DISPATCH |
4. Process Details
Process / Operation | OD grinding |
Outsource | No |
Machine / Cell | Grinding m/c |
Machine / Cell No. | 1 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Man | OD gauge not available. | OD checked by micrometer as OD gauge given for calibration. | X |
Machine | Grinding wheel wear out | Wheel Frequency not defined | X |
6. Inspection Method Analysis (Current)
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | No |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
7. Root Cause Analysis (Occurance)
Why 1 | DIAMETER OVER SIZE-OD O/S & SCRTCH MARK ON OD |
Why 2 | Grinding wheel wear out |
Why 3 | Grinding wheel dressing frequency not defined. |
Why 4 | |
Why 5 | |
Root Cause (Occurance) | Grinding wheel dressing frequency not defined. |
Root Cause Analysis (Outflow)
Why 1 | DIAMETER OVER SIZE-OD O/S & SCRTCH MARK ON OD |
Why 2 | OD Not checked by Gauge |
Why 3 | OD gauge given for calibration. |
Why 4 | Gauge calibration was due. |
Why 5 | |
Root Cause (Outflow) | Gauge calibration was due. |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Outflow | New OD Snap gauge purchased, OD 100 % Check by snap gauge. | Inspector | 25/11/2023 | 27/11/2023 | Completed |
Occurance | Grinding wheel dressing frequency defined after | operator | 25/11/2023 | 27/11/2023 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | No |
Change Details | OD check by snap gauge |
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100 % |
10. Evidance of Countermeasure
Occurance (Before) |
Grinding wheel dressing frequency not defined. 600_Occurance_Before.jpeg |
Occurance (After) |
Grinding wheel dressing frequency defined . 600_Occurance_After.jpeg |
Outflow (Before) |
OD checked by micrometer as OD gauge given for calibration. 600_Outflow_Before.jpeg |
Outflow (After) |
New OD Snap gauge purchased, OD 100 % Check by snap gauge. 600_Outflow_After.jpeg |
11. Horizontal Deployment
Horizontal Deployment Required | No |
Applicable Machine / Model / Plant | Machine,Man |
12. Document Review
Documents | ControlPlan, PFMEA |
Specify Other Document | G.wheel dress.Record |
13. Effectiveness Of Action
Reviewed Quantity | |
Reason for submission |