QFR No - 8000853856
Defect Details
NC No. 8000853856
NC Date 05/12/2023
NC Submission Date
Part No. S2HT52107B
Part Name OUTER SPRING K0PG
Supplier Name & Code 101236-SUMA SPRINGS PRIVATE LIMITED
ETL Plant 1146-ETL Suspension Narasapura
Defect Details MIX UP OTHER MODEL-NOT USING K0PG MODEL MIX UP AT SUMA END
 
1. Problem Description
Defect Description wrong part supplied not using K0PG rear model ( Mix up at supplier end )
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 1
Is Defect Repeatative? Yes
Defect Sketch / Photo sfiqcryk235brvcvwblawxhc.gif
Supplier Communication Details
Quality Head Email ID qc@sumasprings.com
Plant Head/CEO Email ID vp@sumasprings.com
MD Email ID
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
100
0
0
0
0
100
Check Qty
100
0
0
0
0
100
NG Qty
1
0
0
0
0
1
 
Scrap 1
Rework 0
Under Deviation 0
Containment Action
Awareness created to the packing team, Segregated at Customer end as well as Suma End
 
3. Process Flow
Process Flow Description
COILING+TEMP1+GRINDING+SHOTPEEENING+TEMPERING2+SCRAGGING +BEND CHECK AND OILING+PDI+PACKING AND DESPATCH
 
4. Process Details
Process / Operation Packing
Outsource No
Machine / Cell Manual
Machine / Cell No. Manual
5. Problem Analysis
Type Possible Cause Fact Verification Jud
Method.During Packing left over parts of similar parts mixupverifed leftover parts kept in packing stageO
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method visual & tag identfy
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size IS2500-2k
7. Root Cause Analysis (Occurance)
Why 1 Similar part mix-up
Why 2 mix up during packing
Why 3 during Packing left over parts of similar parts mix-up
Why 4
Why 5
Root Cause (Occurance) During Packing left over parts of similar parts mix-up
 
Root Cause Analysis (Outflow)
Why 1 Similar part mix-up
Why 2 Ineffective awareness for packing personnel
Why 3
Why 4
Why 5
Root Cause (Outflow) During Packing left over parts of similar parts mix-up
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceDuring Packing left over parts of similar model will be identified and to be return back to storage areaCHANDRAN07/12/202307/12/2023Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System No
Change Details Nil
Inspection Method Other
Other Inspection Method visual & Tag System
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size IS2500 2K
10. Evidance of Countermeasure
Occurance (Before) During Packing left over parts kept in the packing area
605_Occurance_Before.pdf
Occurance (After) During Packing left over parts of similar model will be identified and to be return back to storage area
605_Occurance_After.pdf
Outflow (Before) Ineffective awareness for packing personnel
605_Outflow_Before.jpeg
Outflow (After) Awareness created to the packing personnel and impact of part mix up explained
605_Outflow_After.jpeg
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant F1GN01102
 
12. Document Review
Documents
Specify Other Document QALERT & AWARENES,
 
13. Effectiveness Of Action
Reviewed Quantity
Reason for submission