QFR No - 8000853856
Defect Details
NC No. | 8000853856 |
NC Date | 05/12/2023 |
NC Submission Date | |
Part No. | S2HT52107B |
Part Name | OUTER SPRING K0PG |
Supplier Name & Code | 101236-SUMA SPRINGS PRIVATE LIMITED |
ETL Plant | 1146-ETL Suspension Narasapura |
Defect Details | MIX UP OTHER MODEL-NOT USING K0PG MODEL MIX UP AT SUMA END |
1. Problem Description
Defect Description | wrong part supplied not using K0PG rear model ( Mix up at supplier end ) |
Detection Stage | Inprocess |
Problem Severity | Fitment |
NG Quantity | 1 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo | sfiqcryk235brvcvwblawxhc.gif |
Supplier Communication Details
Quality Head Email ID | qc@sumasprings.com |
Plant Head/CEO Email ID | vp@sumasprings.com |
MD Email ID |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
100
|
0
|
0
|
0
|
0
|
100
|
Check Qty |
100
|
0
|
0
|
0
|
0
|
100
|
NG Qty |
1
|
0
|
0
|
0
|
0
|
1
|
Scrap | 1 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
Awareness created to the packing team, Segregated at Customer end as well as Suma End |
3. Process Flow
Process Flow Description |
---|
COILING+TEMP1+GRINDING+SHOTPEEENING+TEMPERING2+SCRAGGING +BEND CHECK AND OILING+PDI+PACKING AND DESPATCH |
4. Process Details
Process / Operation | Packing |
Outsource | No |
Machine / Cell | Manual |
Machine / Cell No. | Manual |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Method | .During Packing left over parts of similar parts mixup | verifed leftover parts kept in packing stage | O |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | visual & tag identfy |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | IS2500-2k |
7. Root Cause Analysis (Occurance)
Why 1 | Similar part mix-up |
Why 2 | mix up during packing |
Why 3 | during Packing left over parts of similar parts mix-up |
Why 4 | |
Why 5 | |
Root Cause (Occurance) | During Packing left over parts of similar parts mix-up |
Root Cause Analysis (Outflow)
Why 1 | Similar part mix-up |
Why 2 | Ineffective awareness for packing personnel |
Why 3 | |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | During Packing left over parts of similar parts mix-up |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | During Packing left over parts of similar model will be identified and to be return back to storage area | CHANDRAN | 07/12/2023 | 07/12/2023 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | No |
Change Details | Nil |
Inspection Method | Other |
Other Inspection Method | visual & Tag System |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | IS2500 2K |
10. Evidance of Countermeasure
Occurance (Before) |
During Packing left over parts kept in the packing area 605_Occurance_Before.pdf |
Occurance (After) |
During Packing left over parts of similar model will be identified and to be return back to storage area 605_Occurance_After.pdf |
Outflow (Before) |
Ineffective awareness for packing personnel 605_Outflow_Before.jpeg |
Outflow (After) |
Awareness created to the packing personnel and impact of part mix up explained 605_Outflow_After.jpeg |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | F1GN01102 |
12. Document Review
Documents | |
Specify Other Document | QALERT & AWARENES, |
13. Effectiveness Of Action
Reviewed Quantity | |
Reason for submission |