QFR No - 8000853857
Defect Details
NC No. 8000853857
NC Date 05/12/2023
NC Submission Date
Part No. S2HT52107B
Part Name OUTER SPRING K0PG
Supplier Name & Code 101236-SUMA SPRINGS PRIVATE LIMITED
ETL Plant 1146-ETL Suspension Narasapura
Defect Details DIMN.U/SIZE.-ID LESS ISSUE
 
1. Problem Description
Defect Description K0PG outer spring ID under size issue
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 1
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID qc@sumasprings.com
Plant Head/CEO Email ID vp@sumasprings.com
MD Email ID
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
1000
0
0
0
0
1000
Check Qty
1000
0
0
0
0
1000
NG Qty
1
0
0
0
0
1
 
Scrap 1
Rework 0
Under Deviation 0
Containment Action
Quality awareness created amongst team, Segregation at ETL end as well as Suma End
 
3. Process Flow
Process Flow Description
COILNG + TEMPERING1+GRINDING +SHOT PEENING+TEMPERING 2+SCRAGING+POWDER COATING+PDI+PACKING AND DESPATCH
 
4. Process Details
Process / Operation COILING
Outsource Yes
Machine / Cell COILING CNC
Machine / Cell No. SIMCO,SCM6100+HCS
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MachineEnd coil shiftVerified and found NGO
 
6. Inspection Method Analysis (Current)
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size IS2500-2K
7. Root Cause Analysis (Occurance)
Why 1 ID under size
Why 2 End coil shift
Why 3 Setting part
Why 4 During initial set up
Why 5
Root Cause (Occurance) Setting part
 
Root Cause Analysis (Outflow)
Why 1 ID under size
Why 2 Stage random inspection
Why 3
Why 4
Why 5
Root Cause (Outflow) Stage random inspection
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceSetting part will be scrapped and pit in red box before productionGrinding incharge08/12/202308/12/2023Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details During grinding stage 100 % Visual inspection to verify the end coil shift
Inspection Method Other
Other Inspection Method VisualInspection
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size IS2500-2K
10. Evidance of Countermeasure
Occurance (Before) Setup part scrapped at the end of shift
608_Occurance_Before.docx
Occurance (After) Setup part scrapped immediately
608_Occurance_After.docx
Outflow (Before) Random inspection during grinding stage
608_Outflow_Before.pdf
Outflow (After) 100 % visual inspection during grinding stage
608_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant F1GN101102B (MAIN SPRING)
 
12. Document Review
Documents ControlPlan, ProcessFlowChart, InspCheckSheet
Specify Other Document Q ALERT
 
13. Effectiveness Of Action
Reviewed Quantity
Reason for submission