QFR No - 8000853857
Defect Details
NC No. | 8000853857 |
NC Date | 05/12/2023 |
NC Submission Date | |
Part No. | S2HT52107B |
Part Name | OUTER SPRING K0PG |
Supplier Name & Code | 101236-SUMA SPRINGS PRIVATE LIMITED |
ETL Plant | 1146-ETL Suspension Narasapura |
Defect Details | DIMN.U/SIZE.-ID LESS ISSUE |
1. Problem Description
Defect Description | K0PG outer spring ID under size issue |
Detection Stage | Inprocess |
Problem Severity | Fitment |
NG Quantity | 1 |
Is Defect Repeatative? | No |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | qc@sumasprings.com |
Plant Head/CEO Email ID | vp@sumasprings.com |
MD Email ID |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
1000
|
0
|
0
|
0
|
0
|
1000
|
Check Qty |
1000
|
0
|
0
|
0
|
0
|
1000
|
NG Qty |
1
|
0
|
0
|
0
|
0
|
1
|
Scrap | 1 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
Quality awareness created amongst team, Segregation at ETL end as well as Suma End |
3. Process Flow
Process Flow Description |
---|
COILNG + TEMPERING1+GRINDING +SHOT PEENING+TEMPERING 2+SCRAGING+POWDER COATING+PDI+PACKING AND DESPATCH |
4. Process Details
Process / Operation | COILING |
Outsource | Yes |
Machine / Cell | COILING CNC |
Machine / Cell No. | SIMCO,SCM6100+HCS |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Machine | End coil shift | Verified and found NG | O |
6. Inspection Method Analysis (Current)
Inspection Method | Instrument |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | IS2500-2K |
7. Root Cause Analysis (Occurance)
Why 1 | ID under size |
Why 2 | End coil shift |
Why 3 | Setting part |
Why 4 | During initial set up |
Why 5 | |
Root Cause (Occurance) | Setting part |
Root Cause Analysis (Outflow)
Why 1 | ID under size |
Why 2 | Stage random inspection |
Why 3 | |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | Stage random inspection |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Setting part will be scrapped and pit in red box before production | Grinding incharge | 08/12/2023 | 08/12/2023 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | During grinding stage 100 % Visual inspection to verify the end coil shift |
Inspection Method | Other |
Other Inspection Method | VisualInspection |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | IS2500-2K |
10. Evidance of Countermeasure
Occurance (Before) |
Setup part scrapped at the end of shift 608_Occurance_Before.docx |
Occurance (After) |
Setup part scrapped immediately 608_Occurance_After.docx |
Outflow (Before) |
Random inspection during grinding stage 608_Outflow_Before.pdf |
Outflow (After) |
100 % visual inspection during grinding stage 608_Outflow_After.pdf |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | F1GN101102B (MAIN SPRING) |
12. Document Review
Documents | ControlPlan, ProcessFlowChart, InspCheckSheet |
Specify Other Document | Q ALERT |
13. Effectiveness Of Action
Reviewed Quantity | |
Reason for submission |