QFR No - 8000854205
Defect Details
NC No. 8000854205
NC Date 08/12/2023
NC Submission Date
Part No. 520PP01902
Part Name WHEEL CLUTCH FINISHED UPGRADE
Supplier Name & Code 100656-MADHURA DIE CAST PVT.LTD
ETL Plant 1132-ETL K-226/1 TRANSMISSION
Defect Details HIGHT O/SIZE.-LUG HIGHT OBS 27.6+ AGAINST 26.60 +/-0.1
 
1. Problem Description
Defect Description Lug Height found oversize up to 27.38~27.6 mm against 26.60±0.1 mm
Detection Stage Inprocess
Problem Severity Function
NG Quantity 1
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID madhuradiecast@gmail.com
Plant Head/CEO Email ID madhuradiecast@gmail.com
MD Email ID madhuradiecast@gaikegroup.in
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
1000
500
0
500
500
2500
Check Qty
1000
500
0
500
500
2500
NG Qty
1
0
0
0
500
501
 
Scrap 1
Rework 0
Under Deviation 0
Containment Action
100% Stock segregate at customer end and Supplier end stock.
 
3. Process Flow
Process Flow Description
1.Casting 2.fetling 3. CNC 1st Set-up 4.CNC 2nd Set-up 5.Drilling & Tapping 6.Final Inspection
 
4. Process Details
Process / Operation CNC 2ND SETUP
Outsource No
Machine / Cell CNC
Machine / Cell No. 07
5. Problem Analysis
Type Possible Cause Fact Verification Jud
Machinechuck jaw looseChecked found okO
ManUnskill Operator On machine.Skill Matrix Varified & Found OK.O
ToolInsert got wearChecked found okO
Methodcomponent shiftverified found not ok component shift due to extra material above OD. So face side got more cut.X
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 1:1
7. Root Cause Analysis (Occurance)
Why 1 HIGHT O/SIZE.-LUG HIGHT OBS 27.6+ AGAINST 26.60 +/-0.1
Why 2 Extra cut on resting face of part during cnc 2nd setup machining
Why 3 Part move & come in front side.
Why 4 Because extra material found in Outer dia .
Why 5 Then there is component shift due to extra material above OD. So face side got more cut.
Root Cause (Occurance) Then there is component shift due to extra material above OD. So face side got more cut.
 
Root Cause Analysis (Outflow)
Why 1 HIGHT O/SIZE.-LUG HIGHT OBS 27.6+ AGAINST 26.60 +/-0.1
Why 2 100% Inspection not done
Why 3
Why 4
Why 5
Root Cause (Outflow) Inspection done on sampling basis
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
Outflow1. Training & Awarness given to operator. 2. OPL is displayed. 3.Quality Alert is displayed.QUALITY SUPERVISOR21/12/202320/12/2023Completed
Occurance1. Started 100 % inspection after fettling operation. 2. Correction done in CNC Program ,OD Cut increases.PRODUCTION SUPERVISOR21/12/202320/12/2023Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Started 100 % inspection after fettling operation.
Inspection Method Other
Other Inspection Method VISUAL
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 1:1
10. Evidance of Countermeasure
Occurance (Before) component shift due to extra material above OD. So face side got more cut.
611_Occurance_Before.jpg
Occurance (After) 1. Started 100 % inspection after fettling operation. 2. Correction done in CNC Program ,OD Cut increases.
611_Occurance_After.pdf
Outflow (Before) 100% Inspection not done
611_Outflow_Before.jpg
Outflow (After) 1. Training & Awarness given to operator. 2. OPL is displayed. 3.Quality Alert is displayed.
611_Outflow_After.jpeg
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant NA
 
12. Document Review
Documents ControlPlan, PFMEA, WISOP, InspCheckSheet
Specify Other Document QUALITY ALERT,OPL
 
13. Effectiveness Of Action
Reviewed Quantity 1000
Reason for submission OK-Sustenance to be monitored