QFR No - 8000854205
Defect Details
NC No. | 8000854205 |
NC Date | 08/12/2023 |
NC Submission Date | |
Part No. | 520PP01902 |
Part Name | WHEEL CLUTCH FINISHED UPGRADE |
Supplier Name & Code | 100656-MADHURA DIE CAST PVT.LTD |
ETL Plant | 1132-ETL K-226/1 TRANSMISSION |
Defect Details | HIGHT O/SIZE.-LUG HIGHT OBS 27.6+ AGAINST 26.60 +/-0.1 |
1. Problem Description
Defect Description | Lug Height found oversize up to 27.38~27.6 mm against 26.60±0.1 mm |
Detection Stage | Inprocess |
Problem Severity | Function |
NG Quantity | 1 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | madhuradiecast@gmail.com |
Plant Head/CEO Email ID | madhuradiecast@gmail.com |
MD Email ID | madhuradiecast@gaikegroup.in |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
1000
|
500
|
0
|
500
|
500
|
2500
|
Check Qty |
1000
|
500
|
0
|
500
|
500
|
2500
|
NG Qty |
1
|
0
|
0
|
0
|
500
|
501
|
Scrap | 1 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
100% Stock segregate at customer end and Supplier end stock. |
3. Process Flow
Process Flow Description |
---|
1.Casting 2.fetling 3. CNC 1st Set-up 4.CNC 2nd Set-up 5.Drilling & Tapping 6.Final Inspection |
4. Process Details
Process / Operation | CNC 2ND SETUP |
Outsource | No |
Machine / Cell | CNC |
Machine / Cell No. | 07 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Machine | chuck jaw loose | Checked found ok | O |
Man | Unskill Operator On machine. | Skill Matrix Varified & Found OK. | O |
Tool | Insert got wear | Checked found ok | O |
Method | component shift | verified found not ok component shift due to extra material above OD. So face side got more cut. | X |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | Visual |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 1:1 |
7. Root Cause Analysis (Occurance)
Why 1 | HIGHT O/SIZE.-LUG HIGHT OBS 27.6+ AGAINST 26.60 +/-0.1 |
Why 2 | Extra cut on resting face of part during cnc 2nd setup machining |
Why 3 | Part move & come in front side. |
Why 4 | Because extra material found in Outer dia . |
Why 5 | Then there is component shift due to extra material above OD. So face side got more cut. |
Root Cause (Occurance) | Then there is component shift due to extra material above OD. So face side got more cut. |
Root Cause Analysis (Outflow)
Why 1 | HIGHT O/SIZE.-LUG HIGHT OBS 27.6+ AGAINST 26.60 +/-0.1 |
Why 2 | 100% Inspection not done |
Why 3 | |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | Inspection done on sampling basis |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Outflow | 1. Training & Awarness given to operator. 2. OPL is displayed. 3.Quality Alert is displayed. | QUALITY SUPERVISOR | 21/12/2023 | 20/12/2023 | Completed |
Occurance | 1. Started 100 % inspection after fettling operation. 2. Correction done in CNC Program ,OD Cut increases. | PRODUCTION SUPERVISOR | 21/12/2023 | 20/12/2023 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | Started 100 % inspection after fettling operation. |
Inspection Method | Other |
Other Inspection Method | VISUAL |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 1:1 |
10. Evidance of Countermeasure
Occurance (Before) |
component shift due to extra material above OD. So face side got more cut. 611_Occurance_Before.jpg |
Occurance (After) |
1. Started 100 % inspection after fettling operation.
2. Correction done in CNC Program ,OD Cut increases. 611_Occurance_After.pdf |
Outflow (Before) |
100% Inspection not done 611_Outflow_Before.jpg |
Outflow (After) |
1. Training & Awarness given to operator.
2. OPL is displayed.
3.Quality Alert is displayed. 611_Outflow_After.jpeg |
11. Horizontal Deployment
Horizontal Deployment Required | No |
Applicable Machine / Model / Plant | NA |
12. Document Review
Documents | ControlPlan, PFMEA, WISOP, InspCheckSheet |
Specify Other Document | QUALITY ALERT,OPL |
13. Effectiveness Of Action
Reviewed Quantity | 1000 |
Reason for submission | OK-Sustenance to be monitored |