QFR No - 8000854709
Defect Details
NC No. | 8000854709 |
NC Date | 12/12/2023 |
NC Submission Date | |
Part No. | B2SU01002O |
Part Name | BRAKE HOSE TUBE CLAMP 2 (N282) |
Supplier Name & Code | 100151-EXCELL PRESSINGS |
ETL Plant | 1120-ETL K-226/2 Disc Brakes |
Defect Details | PLATING NOT OK-PLATING NOT OK |
1. Problem Description
Defect Description | PLATING NOT OK-PLATING NOT OK |
Detection Stage | Receipt |
Problem Severity | Aesthetic |
NG Quantity | 308 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | excellpressings.qc@gmai.com |
Plant Head/CEO Email ID | yogesh_vaidya42@yahoo.co.in |
MD Email ID | excellpressings@gmail.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
3000
|
0
|
0
|
3000
|
2000
|
8000
|
Check Qty |
3000
|
0
|
0
|
3000
|
2000
|
8000
|
NG Qty |
393
|
0
|
0
|
0
|
0
|
393
|
Scrap | 0 |
Rework | 393 |
Under Deviation | 0 |
Containment Action |
---|
All the material was checked at ETL end and our end also |
3. Process Flow
Process Flow Description |
---|
After press opeation, plating is done to the parts at M/S Krishna Industries.Then final inspection is done at our end |
4. Process Details
Process / Operation | Plating |
Outsource | Yes |
Machine / Cell | WATT TANK NO 02 |
Machine / Cell No. | WATT TANK NO 02 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Method | Current supply issue on jigs | V blocks copper cathode are hot | O |
6. Inspection Method Analysis (Current)
Inspection Method | Instrument |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 10 |
7. Root Cause Analysis (Occurance)
Why 1 | Less thickness observed below 8 micron |
Why 2 | Current fluctuation observed |
Why 3 | Jigs copper getting hot |
Why 4 | V block getting loosed |
Why 5 | Monthly maintenance was not done |
Root Cause (Occurance) | Current fluctuations due to overheat cathode contact |
Root Cause Analysis (Outflow)
Why 1 | Thickness was not checked |
Why 2 | Visually found Ok |
Why 3 | |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | At our end thickness was not checked |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Current fluctuations caused to lower the thickness | M/S Krishna Industries | 19/12/2023 | 20/12/2023 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | Every lot plating thickness will be checked |
Inspection Method | Instrument |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100 |
10. Evidance of Countermeasure
Occurance (Before) |
v lock loose contact 613_Occurance_Before.jpg |
Occurance (After) |
v block repaired 613_Occurance_After.jpg |
Outflow (Before) |
Plating Not ok to Hose Clamps 613_Outflow_Before.jpg |
Outflow (After) |
Plating OK to Hose clamps 613_Outflow_After.jpg |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | Plating process at Krishna Industries |
12. Document Review
Documents | ControlPlan, PMCheckSheet, JHCheckSheet, InspCheckSheet |
Specify Other Document | FFPA Checksheet |
13. Effectiveness Of Action
Reviewed Quantity | 100 |
Reason for submission | No defect found in latest lot |