QFR No - 8000854709
Defect Details
NC No. 8000854709
NC Date 12/12/2023
NC Submission Date
Part No. B2SU01002O
Part Name BRAKE HOSE TUBE CLAMP 2 (N282)
Supplier Name & Code 100151-EXCELL PRESSINGS
ETL Plant 1120-ETL K-226/2 Disc Brakes
Defect Details PLATING NOT OK-PLATING NOT OK
 
1. Problem Description
Defect Description PLATING NOT OK-PLATING NOT OK
Detection Stage Receipt
Problem Severity Aesthetic
NG Quantity 308
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID excellpressings.qc@gmai.com
Plant Head/CEO Email ID yogesh_vaidya42@yahoo.co.in
MD Email ID excellpressings@gmail.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
3000
0
0
3000
2000
8000
Check Qty
3000
0
0
3000
2000
8000
NG Qty
393
0
0
0
0
393
 
Scrap 0
Rework 393
Under Deviation 0
Containment Action
All the material was checked at ETL end and our end also
 
3. Process Flow
Process Flow Description
After press opeation, plating is done to the parts at M/S Krishna Industries.Then final inspection is done at our end
 
4. Process Details
Process / Operation Plating
Outsource Yes
Machine / Cell WATT TANK NO 02
Machine / Cell No. WATT TANK NO 02
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodCurrent supply issue on jigsV blocks copper cathode are hotO
 
6. Inspection Method Analysis (Current)
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 10
7. Root Cause Analysis (Occurance)
Why 1 Less thickness observed below 8 micron
Why 2 Current fluctuation observed
Why 3 Jigs copper getting hot
Why 4 V block getting loosed
Why 5 Monthly maintenance was not done
Root Cause (Occurance) Current fluctuations due to overheat cathode contact
 
Root Cause Analysis (Outflow)
Why 1 Thickness was not checked
Why 2 Visually found Ok
Why 3
Why 4
Why 5
Root Cause (Outflow) At our end thickness was not checked
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceCurrent fluctuations caused to lower the thicknessM/S Krishna Industries19/12/202320/12/2023Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Every lot plating thickness will be checked
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100
10. Evidance of Countermeasure
Occurance (Before) v lock loose contact
613_Occurance_Before.jpg
Occurance (After) v block repaired
613_Occurance_After.jpg
Outflow (Before) Plating Not ok to Hose Clamps
613_Outflow_Before.jpg
Outflow (After) Plating OK to Hose clamps
613_Outflow_After.jpg
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant Plating process at Krishna Industries
 
12. Document Review
Documents ControlPlan, PMCheckSheet, JHCheckSheet, InspCheckSheet
Specify Other Document FFPA Checksheet
 
13. Effectiveness Of Action
Reviewed Quantity 100
Reason for submission No defect found in latest lot